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	<title>Productivity Portal &#187; Champion Award Winner 2014</title>
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		<title>Productivity improvement in BDN Nozzle manufacturing line</title>
		<link>https://productivity.imtma.in/msdelphi-tvsdiesel/</link>
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		<pubDate>Sat, 17 Jan 2015 08:13:05 +0000</pubDate>
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				<category><![CDATA[2014]]></category>
		<category><![CDATA[Case Studies]]></category>
		<category><![CDATA[Champion Award Winner 2014]]></category>

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		<description><![CDATA[Productivity improvement in BDN Nozzle manufacturing line to meet the sudden increase in customer demand (TML Passenger car and LTV market).]]></description>
				<content:encoded><![CDATA[<div class="imtma-abstract"><img class="alignnone wp-image-811" src="https://productivity.imtma.in/wp-content/uploads/2015/04/04_01_2014AwardImage.jpg" alt="04_01_2014AwardImage" width="750" height="176" /></div>
<div class="imtma-abstract"></div>
<h3 class="imtma-abstract"><strong><span style="color: #3572ad;">Title</span>:</strong> Productivity improvement in BDN Nozzle manufacturing line to meet the sudden increase in customer demand (TML Passenger car and LTV market).</h3>
<div class="imtma-abstract">
<h3><span style="color: #3572ad;"><strong>Company:</strong> </span>Delphi – TVS Diesel systems Ltd</h3>
<h3><span style="color: #3572ad;"><strong>Project initiation date:</strong> </span>10/10/2012</h3>
<h3><span style="color: #3572ad;"><strong>Challenge </strong></span></h3>
<p>Productivity improvements are the need of hour for the BDN nozzle manufacturing line to meet the sudden increase in customer demand from 2800 nos / day to 4000 nos / day . Current capacity of the line is 3000 nos / day. To meet the increased customer demand it requires investment around 4 crores and also high lead time     ( 12 months ) for procurement of new machines. Hence planned to increase the capacity without investment through productivity improvements to meet the increased customer demand.</p>
<p>Also used the takt time vs capacity analysis to identify the above problem.</p>
<h3><span style="color: #3572ad;"><strong>Data Collection</strong></span></h3>
<p>Following data was collected to understand the current status.</p>
<ul>
<li>Customer demand month wise</li>
<li>Process flow</li>
<li>Current capacity of each process</li>
<li>Up time of critical machines</li>
<li>Rejection levels in each process</li>
<li>Current manufacturing system</li>
<li>Current state of layout</li>
<li>Used the lean manufacturing methodology to collect the data like VALUE Stream Mapping, Cycle time study, Material flow – Sting diagram, Trend graph, Histogram/paretto</li>
</ul>
<h3><span style="color: #3572ad;"><strong>Analysis and Solution Development</strong></span></h3>
<p>BDN nozzle manufacturing process consists of 2 stages. Each stage has several sub processes. We have drawn the VSM for each stage to identify the bottle necks in the flow.</p>
<p><strong>Figure 1</strong></p>
<p><strong>Figure 2</strong></p>
<p>The following bottlenecks were identified in the BDN nozzle-manufacturing stream Cycle time is higher than takt time in ECM process</p>
<p>More unwash rejections observed in seat forming process at soft stage resulting FTPR low in downstream processes</p>
<p>Concentricity and linear dimensional issues in OD grinding operation resulting FTPR low in downstream processes.</p>
<p>Up time low in SEIKO ID grinding operation</p>
<p>Batch type production and process type layout is followed in hard stage machining leads to</p>
<p>More material movement</p>
<p>More operator movement for inspection</p>
<p>More handling – re handling</p>
<p>More WIP between process</p>
<p>Difficulties in day-to-day planning</p>
<p>More supervision required</p>
<p>Due to the above constraints it was unable to meet the increased customer demand.</p>
<h3><span style="color: #3572ad;"><strong>Solution</strong></span></h3>
<p>To eliminate the above listed constraints developed the various ideas through CFT approach as below.</p>
<p><strong>Figure 3</strong></p>
<h3><span style="color: #3572ad;"><strong>Implementation</strong></span></h3>
<p><strong>Figure 4</strong></p>
<p><strong>Figure 5</strong></p>
<p><strong>Figure 6</strong></p>
<p><strong>Figure 7</strong></p>
<p><strong>Figure 8</strong></p>
<p>Cellular layout formed by physical arrangement of machines according to the process flow.</p>
<p>Single piece flow between each process, material handling system modified, dedicated inspection facility provided, dedicated team formed from various functions and training given to the team about cellular concepts</p>
<h3><span style="color: #3572ad;"><strong>Sustain</strong></span></h3>
<p>Have standardized the actions taken to sustain the results through Control plan, Operation layout, Drawing Machineries layout document and Engineering change request / process change request</p>
<h3><span style="color: #3572ad;"><strong>Benefits</strong></span></h3>
<p><strong>Figure 9</strong></p>
<p>Elimination of working on Sundays resulted in power units saving – 60000 units/month and manpower saving - 20 people/day</p>
<h3><span style="color: #3572ad;"><strong>Financial benefits</strong></span></h3>
<p><strong>Figure 10</strong></p>
<p>Total cost saving/year - 1.51 crores and investment for new machine – 4 crores avoided</p>
<h3><span style="color: #3572ad;"><strong>Horizontal deployment</strong></span></h3>
<p>Learning of cellular layout concept with single piece flow can be adopted for pump manufacturing stream.</p>
<p>Learning of hard turning operation implemented in pump delivery valve OD turning process.</p>
<h3><span style="color: #3572ad;"><strong>Other inputs</strong></span></h3>
<p>The team implemented cellular layout with the centralized coolant tank and chillers outside the air condition room which helped in creating dust, mist and fumes free environment (EOHS improvement). Operators are voluntarily coming to work in the newly formed layout and also information flow between customer and supplier process is improved. There is substantial increase in morale of workmen in entire nozzle manufacturing stream.</p>
<p><strong>Figure 11</strong></p>
</div>
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