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	<title>Productivity Portal &#187; 2015</title>
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	<description>IMTMA - Productivity Portal</description>
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		<title>TOYOTA KIRLOSKAR AUTO PARTS. (Winner)</title>
		<link>https://productivity.imtma.in/toyota-kirloskar-auto-parts-bangalore/</link>
		<comments>https://productivity.imtma.in/toyota-kirloskar-auto-parts-bangalore/#comments</comments>
		<pubDate>Wed, 08 Mar 2017 12:30:33 +0000</pubDate>
		<dc:creator><![CDATA[Abhishek D]]></dc:creator>
				<category><![CDATA[2015]]></category>
		<category><![CDATA[2016]]></category>

		<guid isPermaLink="false">http://www.productivity.imtma.in/?p=2243</guid>
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			<p style="text-align: center;"><span style="font-size: 18px;"><strong>PRODUCTIVITY IMPROVEMENT IN TRANSMISSION (T/M) ASSEMBLY LINE THROUGH “JISHUKEN” &amp; “LOW COST AUTOMATION (KARAKURI)”</strong></span></p>
<p><span style="font-size: 21px;"><strong>Need for Project</strong></span></p>

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			<p><strong>TKAP Business need: T/M Volume Trend</strong></p>

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			<p><strong>TKAP Labour Cost Trend</strong></p>

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			<p><strong>Impact on Product Cost</strong></p>

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			<p><strong>TKAP Product Cost Target</strong></p>

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			<p><span style="font-size: 21px;"><strong>Approach</strong></span></p>

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			<p><strong>Conventional Methodology for Productivity Improvement (Labour Cost): Automation</strong></p>

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			<p><img class="alignnone size-full wp-image-2117" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs3.jpg" alt="cs3" /></p>

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			<p style="text-align: center;"><strong>DEMERITS</strong></p>
<ul style="list-style: disc;">
<li>SAFETY<br />
- High Power Equp. (LWD or Fatal Accident)</li>
<li>COST<br />
- High Investment &amp; Running cost (Sensors etc)</li>
<li>SPACE:<br />
- Huge Space coverage (Special Barrication)</li>
<li>MAINT:<br />
- Difficult to Trouble shoot (High Maint Cost)</li>
<li>ENVIRONMENT:<br />
- More Actuators &amp; More Energy Consumption<a href="https://productivity.imtma.in/wp-content/uploads/2017/03/cs19.jpg"><img class=" size-full wp-image-2163 alignleft" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs19.jpg" alt="cs19" width="347" height="104" /></a></li>
</ul>

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			<p style="text-align: left;"><strong>Our Philosophy (Concept)</strong></p>
<p style="text-align: center;">Effective utilization of Man hour: Increase Value Added work by Reducing Muda (Waste) &amp;<br />
Supplementary work for Productivity Improvement</p>

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			<img width="823" height="246" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs4.jpg" class=" vc_box_border_grey attachment-full" alt="cs4" />
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			<p><strong>Our Thinking Way</strong>: Collaboration of of Jishuken &amp; LCA for increasing the Value Added Work (reduce CT)</p>

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			<img width="842" height="316" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs5.jpg" class=" vc_box_border_grey attachment-full" alt="cs5" />
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			<p><strong>Project Planning</strong></p>
<p>Case Study: <strong>T/M Main Assembly &amp; Tester line Productivity Improvement activity</strong></p>
<p><img class=" size-full wp-image-2124 aligncenter" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs6.jpg" alt="cs6" width="847" height="304" /></p>

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			<p><strong>Project Target: 15% Productivity Improvement through CT Reduction (Man loop reduction)</strong></p>
<p><img class=" size-full wp-image-2125 aligncenter" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs7.jpg" alt="cs7" width="832" height="303" /></p>

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			<p><span style="font-size: 21px;"><strong>Project Implementation*</strong></span></p>
<p style="text-align: right;"><span style="font-size: 12px;">* Project implemented from July’14 to Jan’15 (6 Months)</span></p>
<p>It's a Japanese word which means "Self Learning to improve Self (HRD) &amp; Workplace by Eliminating 3M's."</p>
<p><strong>Objectives of Jishuken:</strong><br />
i) Enhance problem solving skill by teamwork<br />
ii) Productivity improvement by Tackling and Eliminating 3Ms<br />
iii) Promote TPS skill up (HRD of Members)</p>
<p><img class=" size-full wp-image-2126 aligncenter" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs8.jpg" alt="cs8" width="818" height="200" /></p>

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			<p><strong>Jishuken Implementation</strong></p>
<p><img class=" size-full wp-image-2130 aligncenter" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs9.jpg" alt="cs9" width="564" height="713" /></p>

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			<p><span style="font-size: 21px;"><strong>Project Implementation</strong></span></p>
<p><strong>What is Low Cost Automation (LCA) – TKAP Definition..?</strong></p>
<p>A System where Man &amp; Machine Collaborate &amp; Work together (No Separation), which meets Expectations of Toyota Way.</p>
<p><strong><img class=" size-full wp-image-2133 aligncenter" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs10.jpg" alt="cs10" width="806" height="399" /></strong></p>
<p><strong>TKAP tool for LCA : "KARAKURI"</strong></p>

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			<p><strong>What is KARAKURI?</strong></p>
<p style="text-align: center;">It's a Japanese word which means "Achieving motion with No Power or Low power (use counter weight,<br />
rope &amp; pulley mechanism).</p>
<p><strong>Why KARAKURI?</strong></p>
<p><img class=" size-full wp-image-2135 aligncenter" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs11.jpg" alt="cs11" /></p>

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			<p><strong>Low Cost Automation (LCA) Implementation</strong></p>
<p>Challenge: Conventional Automation V/S TKAP Low Cost Automation (Karakuri)<br />
<img class="alignnone size-full wp-image-2137" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs12.jpg" alt="cs12" /></p>

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			<p><strong>LCA Innovation &amp; Breakthrough Ideas: After Implementation (in continuation with Jishuken)</strong></p>
<p><img class="alignnone  wp-image-2147" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs13.jpg" alt="cs13" /></p>
<p><img class=" size-full wp-image-2149 aligncenter" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs14.jpg" alt="cs14" /></p>

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			<p><strong>Types of Karakuri at TKAP</strong></p>
<p><img class="alignnone size-full wp-image-2151" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs15.jpg" alt="cs15" /></p>

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			<p><strong>Competitiveness Sustainability through Innovation &amp; Continuous Kaizen</strong></p>
<p><img class="alignnone size-full wp-image-2158" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs16.jpg" alt="cs16" /></p>
<p><img class="alignnone size-full wp-image-2158" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs17.jpg" alt="cs16" /></p>
<p><img class="alignnone size-full wp-image-2161" src="https://productivity.imtma.in/wp-content/uploads/2017/03/cs18.jpg" alt="cs18" width="842" height="429" /></p>
<p>&nbsp;</p>

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		<title>WABCO INDIA LIMITED</title>
		<link>https://productivity.imtma.in/wabco-india-limited/</link>
		<comments>https://productivity.imtma.in/wabco-india-limited/#comments</comments>
		<pubDate>Tue, 20 Sep 2016 11:59:01 +0000</pubDate>
		<dc:creator><![CDATA[Abhishek D]]></dc:creator>
				<category><![CDATA[2015]]></category>

		<guid isPermaLink="false">http://www.productivity.imtma.in/?p=1569</guid>
		<description><![CDATA[Title of case study: Layout transformation and Space Productivity at WABCO AMBATTUR site for future business needs Project implementation start and end date: 13th Oct 2014 to 27th Nov 2014 Is it in continued operation now?: Yes Innovation: Elaborate in detail...]]></description>
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	</div> <span style="color: #3572ad;"><strong>Title of case study:</strong></span><br />
Layout transformation and Space Productivity at WABCO AMBATTUR site for future business needs</p>
<p><span style="color: #3572ad;"><strong>Project implementation start and end date:</strong></span><br />
13th Oct 2014 to 27th Nov 2014</p>
<p><span style="color: #3572ad;"><strong>Is it in continued operation now?:</strong></span> Yes</p>
<p><span style="color: #3572ad;"><strong>Innovation: Elaborate in detail as to how your project stands out for its uniqueness / innovation</strong></span></p>
<ul>
<li>The purpose of any productivity improvement project is not only to increase the numbers produced in any particular cell / line but also to ensure that the current productivity project address the company’s current important business problem.</li>
<li>In that case, there could be sometimes where the project selection is directly driven from the business need and this project is one among it.</li>
<li>The innovation in the project explained in the case study is that the usage of various simulation ideas using spaghetti charts, “CUT” &amp; “PASTE” brainstorming sessions with leadership team to the “Real” scale, Business vs space occupancy, Production density concepts etc.</li>
<li>Entitled to deliver additional space for the business need, the methodology adopted is not only limited to the layout and flow but also to the application of ECRS in process &amp; product engineering as well where the status quo was challenged (creation of mixed model cell, challenging low volume stranger products portfolio)</li>
<li>Entitled to deliver additional space for the business need, the methodology adopted is not only limited to the layout and flow but also to the application of ECRS in process &amp; product engineering as well where the status quo was challenged (creation of mixed model cell, challenging low volume stranger products portfolio)</li>
</ul>
<p><span style="color: #3572ad;"><strong>Problem identification: Why was this problem selected? What methodology was adopted to identify the problem?</strong></span></p>
<ul>
<li>WABCO INDIA LIMITED, Ambattur plant (which started its operations in 2006) is proposed to double the sales turnover in the upcoming four years with entry of new technology global products from WABCO.<br />
?Totally with 50 machining cells &amp; 78 assembly cells in an overall shop floor area of 10676 Sq.m, the floor is already filled up with new products till 2013H2 and hardly a free space available for new assemblies &amp; machining lines since then.</li>
<li>The Ambattur plant is a single roof factory where the entire production floor and the office areas including WABCO INDIA’s product development team, production engineering team and other central functions are having its operation.</li>
<li>With a required additional area of 1800 Sq.m for new products, it was earlier decided to augment the free space either through shifting the entire factory to outskirts of Chennai leaving behind the Ambattur facility as R&amp;D center or to move some of the key assembly and machining cells to our Jamshedpur facility compromising on the increased logistics cost of raw material &amp; finished goods movement from the major supplier / customer base in the south.</li>
<li>However, considering the business importance &amp; the massive cost impact on new facility / shifting, a cross functional team is formed led by Lean Promotion office with a very strong entitlement to create the required space in the existing facility through layout transformation &amp; space productivity<img class="alignnone wp-image-1577 size-full" src="https://productivity.imtma.in/wp-content/uploads/2016/09/wabco_inno1.png" alt="wabco_inno1" width="399" height="300" /></li>
</ul>
<p><span style="color: #3572ad;"><strong>Data collection: What data was collected? What methodology was adopted to collect the data?</strong></span></p>
<ul>
<li style="margin-left: 20px;">Current space utilization (CAPACITY utilization)<br />
Total Built up area : 47451 Sq.m<br />
Shop floor area : 10676 Sq.m<br />
Current shop floor utilization (%) : 68.82%<br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/wabco_iData-collection1.png"><img class="alignnone size-full wp-image-1578" src="https://productivity.imtma.in/wp-content/uploads/2016/09/wabco_iData-collection1.png" alt="wabco_idata-collection1" width="324" height="196" /></a></li>
<li>New products pipeline details &amp; the corresponding space / draft layout plan required
<div class="new_pro_tbl">
<table>
<tbody>
<tr>
<td colspan="2" width="126"><strong><b> </b></strong></td>
<td colspan="6" width="268"><strong><b>New space required in Sq.m</b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>Sl No</b></strong></td>
<td width="91"><strong><b> Product</b></strong></td>
<td width="44"><strong><b>2014</b></strong></td>
<td width="44"><strong><b>2015</b></strong></td>
<td width="44"><strong><b>2016</b></strong></td>
<td width="44"><strong><b>2017</b></strong></td>
<td width="44"><strong><b>2018</b></strong></td>
<td width="44"><strong><b>2019</b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>1</b></strong></td>
<td width="91"><strong><b>Air tank</b></strong></td>
<td width="44"><strong><b>+134</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>2</b></strong></td>
<td width="91"><strong><b>ABS</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b>+499</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>3</b></strong></td>
<td width="91"><strong><b>AMT</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b>+198</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>4</b></strong></td>
<td width="91"><strong><b>ADB</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b>+112</b></strong></td>
<td width="44"><strong><b>+170</b></strong></td>
<td width="44"><strong><b>+200</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>5</b></strong></td>
<td width="91"><strong><b>3.5” CS</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b>+186</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>6</b></strong></td>
<td width="91"><strong><b>Vac.Pump</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b>+161</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
</tr>
<tr>
<td width="35"><strong><b>7</b></strong></td>
<td width="91"><strong><b>Others </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b>+170</b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"><strong><b> </b></strong></td>
<td width="44"></td>
</tr>
</tbody>
</table>
</div>
</li>
<li>Details of monuments in the layout (Like Pillar, Structures, trusses, wash etc) &amp; machine layout (with real time GEMBA validation &amp; methodologies) for all the machines of the sub-scope</li>
<li>For existing products, current flow, business demand for the upcoming years, current cell utilization (%), Size of the product in order to analyze the demand (vs) size distribution.</li>
</ul>
<div style="margin-left: 15px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/DEMAND.bmp"><img class="alignnone size-full wp-image-1587" src="https://productivity.imtma.in/wp-content/uploads/2016/09/DEMAND.bmp" alt="demand" width="698" height="518" /></a></div>
<p>&nbsp;</p>
<p><span style="color: #3572ad;"><strong>Analysis and development of solution: What analysis was done? What alternate solutions were identified? Why was this particular solution chosen?</strong></span></p>
<ul>
<li>Based on the current space utilization and CAPACITY utilization the cells were categorized and locations of the cells were mapped.</li>
<li>The first step is to arrange the cells accordingly to the demand of the product by shifting high runners and big products near to the raw material warehouse. By doing such optimization the layout of the cells were challenged and cell sizes are reduced by the application of ECRS.</li>
</ul>
<div style="margin-left: 20px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/celllocation.bmp"><img class="alignnone size-full wp-image-1590" src="https://productivity.imtma.in/wp-content/uploads/2016/09/celllocation.bmp" alt="celllocation" width="614" height="464" /></a></div>
<div style="margin-left: 20px;"></div>
<ul>
<li>For low volume repeaters and stranger cells (huge size) which occupies more space, in phase I the cells were relocated away from raw material stores. Similarly by doing such optimization the layout has been challenged with the following strategies</li>
</ul>
<ul style="margin-left: 40px;">
<li>Strategy I - For cells with less than 25% capacity utilization, rationalize the product with existing runner products and eliminate the line hence releasing space.</li>
<li>Strategy II – For cells with 25-40% capacity utilization it is proposed to combine the cell with other runner assembly cells to create a “Mixed-Model” cell with minimum / no set-up time.</li>
<li>There were totally 9 projects that were identified under the above said strategies out of the entire assembly shop accounting for 250 Sq.m</li>
</ul>
<div style="margin-left: 35px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/reality.bmp"><img class="alignnone size-full wp-image-1602" src="https://productivity.imtma.in/wp-content/uploads/2016/09/reality.bmp" alt="reality" width="515" height="393" /></a></div>
<ul>
<li>On the other hand, for machining layout, the current state layout has been captured &amp; the same has been scaled down to the corresponding sizes for real time – simulation scenarios. And detailed spaghetti charts were prepared to understand &amp; analyze the existing flow</li>
<li>Aligning with the business need &amp; the space occupation % in the overall layout, the unit for implementation of the layout has been chosen. For instance, the C&amp;B1 unit with 3 product families, 7 MIW products in 131 variants that is manufactured across 20 machining cells occupying an overall 3200 Sq.m has been selected.</li>
<li>An entitlement layout has been arrived along with the leadership and four cross functional workshops were conducted where the real time scenarios were simulated and the ideal layout scenarios has been chosen based on optimal KPIs (key performance indicators)</li>
</ul>
<div style="margin-left: 40px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/scaledbig.bmp"><img class="alignnone size-full wp-image-1608" src="https://productivity.imtma.in/wp-content/uploads/2016/09/scaledbig.bmp" alt="scaledbig" width="734" height="769" /></a></div>
<p><span style="color: #3572ad;"><strong>Implementation: How was the chosen solution tested/validated and implemented? </strong></span></p>
<ul>
<li>To begin with, an overall entitlement out of the layout transformation has been set with KPI’S as follows.</li>
</ul>
<div style="margin-left: 35px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/transformation.bmp"><img class="alignnone size-full wp-image-1613" src="https://productivity.imtma.in/wp-content/uploads/2016/09/transformation.bmp" alt="transformation" width="500" height="601" /></a></div>
<div style="margin-left: 35px;"></div>
<ul>
<li>As discussed in the previous sections, various scenarios have been identified through the layout simulation workshops, and each of them was validated upon the impact they have in the KPI’s of the layout entitlement. In some cases of challenging the locations of very big machines such as honing, grinding, 5 axis horizontal machining centers, plasma nitriding a detailed criteria evaluation has been done once before the final location on the layout has been arrived.</li>
</ul>
<div style="margin-left: 40px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/big-machines.bmp"><img class="alignnone size-full wp-image-1619" src="https://productivity.imtma.in/wp-content/uploads/2016/09/big-machines.bmp" alt="big-machines" width="500" height="600" /></a></div>
<div style="margin-left: 40px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/evelucation.bmp"><img class="alignnone size-full wp-image-1623" src="https://productivity.imtma.in/wp-content/uploads/2016/09/evelucation.bmp" alt="evelucation" width="500" height="605" /></a></div>
<div style="margin-left: 40px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/criteria.bmp"><img class="alignnone size-full wp-image-1626" src="https://productivity.imtma.in/wp-content/uploads/2016/09/criteria.bmp" alt="criteria" width="700" height="604" /></a></div>
<div style="margin-left: 40px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/design.bmp"><img class="alignnone size-full wp-image-1630" src="https://productivity.imtma.in/wp-content/uploads/2016/09/design.bmp" alt="design" width="500" height="600" /></a></div>
<ul>
<li>As the overall layout optimization in the machine shop involves comparatively higher man-days on shifting, the festival-off time of Nov’14 was chosen to implement the total layout optimization</li>
<li>In the layout optimization, OLD MACHINES (on an average life of &gt;30 years), with bulky ATC mechanism were made more space efficient by ECRS methodology in the process to eliminate the machine &amp; offload the operations without affecting productivity (total 4 machines in the same case – accounts to 250 Sq.m)</li>
<li>Big machines which were GANGWAY specific (HR3A – 4 machines, Honing – 2 machines – Width of the machines &gt; 3 meters ) were challenged for improved space efficiency &amp; production density by utilization of vertical space for accessories (Totally 5 similar kaizen ideas were implemented during the optimization process which have converted the “machines” as “Gangway-specific” &amp; not the “gangways” as “Machine – Specific</li>
<li>Totally 20 hours of layout optimization has happened over 2 weeks of time with total 48 machines repositioned according to the layout plan with 12 machines challenged for space efficiency &amp; improved production density.</li>
<li>After the total layout revamping, the entire exercise has been re-validated for the process capability of all the critical parameters &amp; found the sustenance of it above 2</li>
<li>In assembly, the selected projects were implemented as per the schedule with necessary customer / PPAP approvals.</li>
<li>For project that involved the rationalization of the product portfolio, the Quality team was made to visit the field to validate the application of the proposed products</li>
</ul>
<p><span style="color: #3572ad;"><strong>Benefits to organization:</strong></span><br />
<span style="color: #3572ad;"><strong>Operational benefits: What benefits were accrued to the organization as a result of the implementation of the project? </strong></span></p>
<ul>
<li>Generation of free space – 1260 Sq.m (12% of the shop floor area)</li>
<li>Non-cyclical Headcount reduction – 3 operators / shift</li>
<li>Reduction in average material travel distance by 28%</li>
<li>Single piece flow has been ensured in all the cells that undergone layout transformation.</li>
<li>Standardized the Gangways hence, Gangway specific machines rather than machine specific gangway.</li>
</ul>
<p><span style="color: #3572ad;"><strong>Financial benefits: Describe the financial benefits on parameters such as cost saving, avoidance of CAPEX, etc. as relevant to this project.</strong></span></p>
<ul>
<li>Generation of free space thereby potentially averted the need for the expansion of the plant resulting in savings 640 lacs one time.</li>
<li>Released totally 4 old HMC’s resulting in CAPEX avoidance of 240 lacs for new machines.</li>
<li>Ensured productivity improvement of 20% indirectly through layout optimization in two cells (HINO crankcase machining cell &amp; WC crankcase machining cell) without any other investment.</li>
<li>WIP inventory reduction of 18 lacs through inventory points reduction &amp; ensuring single piece flow.</li>
<li>Savings / annum on reduction of 3 operators / shift : 7.2 lacs p.a</li>
</ul>
<p><span style="color: #3572ad;"><strong>Institutionalization and horizontal deployment, if any: </strong></span></p>
<ul>
<li>The entire layout is standardized after the major revamping &amp; the same is been owned now by LPO (Lean Promotion office).</li>
<li>The cpk has been validated for critical Quality parameters after the layout transformation.</li>
<li>Any changes in the layout hereinafter system is created in such a way that, a cross functional workshop is been conducted involving all the stakeholders will be planned to evaluate the various scenarios &amp; to choose the ideal one.</li>
<li>Now the horizontal deployment is on-going in crankshaft machining cells of C&amp;B1 unit</li>
<li>The entire project of space productivity in our site has not only involved the conventional way of creating the free space by some kaizens but also it featured a companywide approach to de-fragment the existing layout through identification of projects from every manufacturing units and deployment of the targets to them. While creation of the free space, the entire layout of the site is aligned to the designed ideal future state layout with improved flow thereby creating a layout transformation. In few cases both the existing process design &amp; product design has been challenged and a committed cross functions involving R&amp;D, Marketing &amp; Field service were also involved.</li>
</ul>
<p>&nbsp;</p>
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		<title>TVS MOTOR Co. Ltd</title>
		<link>https://productivity.imtma.in/tvs-motor-co-ltd/</link>
		<comments>https://productivity.imtma.in/tvs-motor-co-ltd/#comments</comments>
		<pubDate>Tue, 20 Sep 2016 10:09:58 +0000</pubDate>
		<dc:creator><![CDATA[Abhishek D]]></dc:creator>
				<category><![CDATA[2015]]></category>

		<guid isPermaLink="false">http://www.productivity.imtma.in/?p=1643</guid>
		<description><![CDATA[Title of case study: Productivity improvement and flow manufacturing in machining fixtures and gauges through innovation and design standardization. Project implementation start and end date: March 2012 to January 2013 Is it in continued operation now? Yes Certificate of the...]]></description>
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	</div> 

	<div class="wpb_text_column wpb_content_element ">
		<div class="wpb_wrapper">
			
		</div> 
	</div> <span style="color: #3572ad;"><strong>Title of case study:</strong></span><br />
Productivity improvement and flow manufacturing in machining fixtures and gauges through innovation and design standardization.</p>
<p><span style="color: #3572ad;"><strong>Project implementation start and end date:</strong></span><br />
March 2012 to January 2013</p>
<p><span style="color: #3572ad;"><strong>Is it in continued operation now?</strong></span> Yes</p>
<p><span style="color: #3572ad;"><strong>Certificate of the division/business/unit/company head</strong></span></p>
<ul>
<li>We certify that the productivity improvement project described here was implemented by the above team and is in continuous operation. We also certify that the claimed benefits accrued to our organization. We also agree that the contents of this case study can be published by the organizers.</li>
<li>Cost saving from this project: 37 Lacs*.</li>
</ul>
<p><span style="color: #3572ad; margin-left: 40px;"><strong> PART-A MACHINING FIXTURES</strong></span><br />
<span style="color: #3572ad;"><strong>Innovation:</strong></span><br />
<span style="color: #3572ad;"><strong>Machining Fixtures</strong></span></p>
<ul>
<li>We have conceived, designed, manufactured and implemented next generation machining fixtures. We call them chip-less and clamp-less fixtures. The fixture elements have been indigenously designed by us resulting in low cost &amp; better reliability.</li>
</ul>
<ul>
<li>1)Provided unique 4 in 1 functional unit that is used to locate orient, rest &amp; clamp the part. This has been indigenously designed and developed by us.</li>
</ul>
<div style="margin-left: 300px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/4-in-1sm.bmp"><img class="alignnone size-full wp-image-1647" src="https://productivity.imtma.in/wp-content/uploads/2016/09/4-in-1sm.bmp" alt="4-in-1sm" width="71" height="57" /></a></div>
<ul>
<li>2)Spherical base plate to ensure no chip accumulation during processing</li>
</ul>
<div style="margin-left: 300px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/Spherical.bmp"><img class="alignnone size-full wp-image-1657" src="https://productivity.imtma.in/wp-content/uploads/2016/09/Spherical.bmp" alt="spherical" width="71" height="90" /></a></div>
<ul>
<li>3)Obstruction to componentloading/unloading In fixture eliminated through clamp-less fixtures</li>
</ul>
<div style="margin-left: 300px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/Obstruction.bmp"><img class="alignnone size-full wp-image-1658" src="https://productivity.imtma.in/wp-content/uploads/2016/09/Obstruction.bmp" alt="obstruction" width="175" height="121" /></a></div>
<ul>
<li>4)Fixture parts life improvement through Special coating which is maintenance free</li>
</ul>
<ul>
<li>5)Lead time reduction through parts reduction &amp; standardization</li>
</ul>
<div style="margin-left: 300px;"><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/reduction1.bmp"><img class="alignnone size-full wp-image-1659" src="https://productivity.imtma.in/wp-content/uploads/2016/09/reduction1.bmp" alt="reduction1" width="54" height="57" /></a></div>
<p><span style="color: #3572ad;"><strong> Problem identification:</strong></span></p>
<ul>
<ul>Considering the short time for any product to market and increasing number of new projects owing to shorter product life cycle, it becomes very critical to shorten the time of production facility creation (fixtures, gauges, machines, tools etc.)</ul>
</ul>
<ul>
<li>Multi model facility creation is the need of the hour.</li>
<li>Also effective utilization of the established production facilities is critical (minimizing losses &amp; enhancing productivity)</li>
<li>In Star family where the production volume is higher, we observed</li>
</ul>
<ul style="margin-left: 80px;">
<li>Low employee productivity</li>
<li>Lead time high for fixture availability</li>
<li>More part damages in handling</li>
</ul>
<p><span style="color: #3572ad;"><strong>Close observation of the operator working, revealed following difficulties.</strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/Machining-fixture.bmp"><img class="alignnone size-full wp-image-1662" src="https://productivity.imtma.in/wp-content/uploads/2016/09/Machining-fixture.bmp" alt="machining-fixture" width="188" height="188" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/Various-Operations.bmp"><img class="alignnone size-full wp-image-1663" src="https://productivity.imtma.in/wp-content/uploads/2016/09/Various-Operations.bmp" alt="various-operations" width="225" height="181" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/component.bmp"><img class="alignnone size-full wp-image-1664" src="https://productivity.imtma.in/wp-content/uploads/2016/09/component.bmp" alt="component" width="296" height="158" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/chart.bmp"><img class="alignnone size-full wp-image-1665" src="https://productivity.imtma.in/wp-content/uploads/2016/09/chart.bmp" alt="chart" width="457" height="262" /></a></center><span style="color: #3572ad;"><strong>Data collection: </strong></span></p>
<ul>
<li>The following data were collected for the identified machining cells pertaining to machining fixtures &amp; gauges (Source: Star family)</li>
</ul>
<ul>
<li>a)Part damage details due to handling</li>
<li>b)Repairing time (MTTR)</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/part.bmp"><img class="alignnone size-full wp-image-1672" src="https://productivity.imtma.in/wp-content/uploads/2016/09/part.bmp" alt="part" width="206" height="138" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/repairing.bmp"><img class="alignnone size-full wp-image-1673" src="https://productivity.imtma.in/wp-content/uploads/2016/09/repairing.bmp" alt="repairing" width="220" height="139" /></a></center><br />
<span style="color: #3572ad;"><strong>Analysis and development of solution</strong></span></p>
<ul>
<li>We used Advance 5-s technique &amp; 7 QC tools to challenge our current practices and go for a next generation fixtures.</li>
</ul>
<p><center><span style="color: #3572ad;"><strong>Advanced 5S technique</strong></span></center><br />
<strong><b>     5s of a Fixture: </b></strong></p>
<ul>
<li><strong><b> Sort Out –     </b></strong><strong><b>Identify/</b></strong><strong><u><b>eliminate</b></u></strong><strong><b> the undesired factors.</b></strong></li>
<li><strong><b> Set Limit –     </b></strong><strong><b>Identify/incorporate the </b></strong><strong><u><b>basic requirements </b></u></strong><strong><b>of fixtures.</b></strong><b></b></li>
<li><strong><b> Shine –             </b></strong><strong><b>List out the </b></strong><strong><u><b>best in its class ideas </b></u></strong><strong><b>for enhancing the  </b></strong><strong><b>                             </b></strong><strong><b>functionality of fixtures.</b></strong></li>
</ul>
<ul>
<li><strong><b>Standardize -  </b></strong><strong><b>Shine ideas generated to be </b></strong><u></u></li>
<li><strong><b>Sustain –  </b></strong><strong><b>Improvement made to be made </b></strong></li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/table.bmp"><img class="alignnone size-full wp-image-1679" src="https://productivity.imtma.in/wp-content/uploads/2016/09/table.bmp" alt="table" width="432" height="229" /></a></center><span style="color: #3572ad;"><strong>implementation</strong></span></p>
<p>The next generation fixtures were tested&amp; validated</p>
<ul>
<li>a)Verified in our alpha shop for the actual process parameters with 500 no components and all quality parameters were inspected.</li>
<li>b) Validated in the actual production cell.</li>
<li>c) Customer voice captured</li>
<li>d) MFMEA for design standardization</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/image_big.bmp"><img class="alignnone size-full wp-image-1680" src="https://productivity.imtma.in/wp-content/uploads/2016/09/image_big.bmp" alt="image_big" width="432" height="243" /></a></center><span style="color: #3572ad;"><strong>Benefits to organization:</strong></span></p>
<ul>a) Operational benefits:</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/operational.bmp"><img class="alignnone size-full wp-image-1681" src="https://productivity.imtma.in/wp-content/uploads/2016/09/operational.bmp" alt="operational" width="426" height="238" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/chart1.bmp"><img class="alignnone size-full wp-image-1682" src="https://productivity.imtma.in/wp-content/uploads/2016/09/chart1.bmp" alt="chart1" width="441" height="347" /></a></center></p>
<ul>b) Operational benefits:</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/1.bmp"><img class="alignnone size-full wp-image-1683" src="https://productivity.imtma.in/wp-content/uploads/2016/09/1.bmp" alt="1" width="210" height="139" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/2.bmp"><img class="alignnone size-full wp-image-1684" src="https://productivity.imtma.in/wp-content/uploads/2016/09/2.bmp" alt="2" width="207" height="146" /></a></center><br />
<span style="color: #3572ad; margin-left: 250px;"><strong> PART-B- GAUGES</strong></span><br />
<span style="color: #3572ad;"><strong> Innovation: </strong></span></p>
<ul>We have gone for sub-system standardization. This has helped us reduce the number of distinct parts to be designed. Also integrated the standard catalogue parts into our design for improving the gauges R&amp;R &amp; cost reduction (eg, Misumi, THK etc). Able to maintain off the shelf standard parts so that the time to manufacturing is greatly reduced.</ul>
<p><span style="color: #3572ad;"><strong> Problem identification </strong></span></p>
<p>Design, procurement, manufacturing and implementation are the 4 main phases of facility creation for any project<br />
We also observed that there was a high lead time to design critical gauges (2-6 weeks) and high lead time in manufacturing &amp; making them available<br />
(6-10 weeks)<br />
Any new project requires 6M facilities. This project was selected based on our pareto for facility creation.</p>
<p><span style="color: #3572ad;"><strong> Pareto indicating the importance of gauges availability for any new project. </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/facilities.bmp"><img class="alignnone size-full wp-image-1686" src="https://productivity.imtma.in/wp-content/uploads/2016/09/facilities.bmp" alt="facilities" width="449" height="211" /></a></center><span style="color: #3572ad;"><strong> Data collection: </strong></span></p>
<p>The following data were collected for the identified machining cells pertaining to machining fixtures &amp; gauges (Source: Star family)<br />
a) Types of gauges, their lead time to availability<br />
b) Stratification of lead time data</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/3.bmp"><img class="alignnone size-full wp-image-1688" src="https://productivity.imtma.in/wp-content/uploads/2016/09/3.bmp" alt="3" width="430" height="135" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/5.bmp"><img class="alignnone size-full wp-image-1689" src="https://productivity.imtma.in/wp-content/uploads/2016/09/5.bmp" alt="5" width="508" height="157" /></a></center>&nbsp;</p>
<p><span style="color: #3572ad;"><strong>Analysis and development of solution</strong></span></p>
<p>The following data were collected for the identified machining cells pertaining to machining fixtures &amp; gauges (Source: Star family)</p>
<ul style="margin-left: 50px;">
<li>We used root cause analysis for more lead time in gauges availability through brainstorming.</li>
<li>We did a cost impact analysis item wise for critical gauges.</li>
<li>Also did the repetitive designs in critical gauges.</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/6.bmp"><img class="alignnone size-full wp-image-1691" src="https://productivity.imtma.in/wp-content/uploads/2016/09/6.bmp" alt="6" width="432" height="206" /></a></center><br />
<span style="color: #3572ad;"><strong>Implementation</strong></span></p>
<p>Sub-system level standardization has been extended to all gauges of Camshaft, Frame, Panel checkers etc. MFMEA was conducted to ascertain the performance of these gauges. 2 gauges were manufactured to test and ascertain the same. Also designed with an eye to use readily available parts<br />
eg. LM guide for front sliding motion.(from MISUMI)</p>
<p>a) Parts commonised for the transmission part gauges:.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/7.bmp"><img class="alignnone size-full wp-image-1693" src="https://productivity.imtma.in/wp-content/uploads/2016/09/7.bmp" alt="7" width="301" height="225" /></a></center><br />
b) Sub-system standardized for all the similar fabrication gauges:</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/8.bmp"><img class="alignnone size-full wp-image-1694" src="https://productivity.imtma.in/wp-content/uploads/2016/09/8.bmp" alt="8" width="391" height="190" /></a></center><br />
c)Bought-out part used for substituting designed elements:</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/9.bmp"><img class="alignnone size-full wp-image-1695" src="https://productivity.imtma.in/wp-content/uploads/2016/09/9.bmp" alt="9" width="383" height="213" /></a></center><br />
<span style="color: #3572ad;"><strong>Benefits to organization:</strong></span><br />
<span style="color: #3572ad;"><strong>a)Operational benefits</strong></span></p>
<ul style="margin-left: 50px;">
<li>50%Productivity of our designers enhanced from 100 designs/man/year to 150 designs/man year</li>
<li>Overall gauge handing over time reduced to 10 weeks.<br />
Design lead time reduced from 6 weeks to 4 weeks for critical gauges</li>
</ul>
<p><span style="color: #3572ad;"><strong>Financial benefits:</strong></span></p>
<p>Cost saving owing to standardization - 20%<br />
This is by using standard parts with simplified designs.<br />
Designs are patented.<br />
Cost certificate attached in total in pg.5: - Total saving 37 Lacs for one model of fixtures and gauges.</p>
<p><span style="color: #3572ad;"><strong>Institutionalization and horizontal deployment, if any</strong></span></p>
<p>Please elaborate on how the changes have been embedded in the system and horizontally deployed as applicable.</p>
<p><span style="color: #3572ad;"><strong>This is for the total case study (Part A &amp; Part B)</strong></span></p>
<p>We have deployed 17 nos. of next generation fixtures across star models.<br />
Our design shine points have been communicated to all &amp; are being ensured that the new machining fixtures are complying with the same.<br />
Gauges &amp; fixtures standard parts created &amp; are being used for all projects after implementation.<br />
Design manuals &amp; guidelines updated. Suppliers are supplying gauges &amp; fixtures as per these guidelines.</p>
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		<title>KEIHINFIE PVT. LTD</title>
		<link>https://productivity.imtma.in/ms-keihinfie-pvt-ltd/</link>
		<comments>https://productivity.imtma.in/ms-keihinfie-pvt-ltd/#comments</comments>
		<pubDate>Tue, 20 Sep 2016 07:35:47 +0000</pubDate>
		<dc:creator><![CDATA[Abhishek D]]></dc:creator>
				<category><![CDATA[2015]]></category>

		<guid isPermaLink="false">http://www.productivity.imtma.in/?p=1754</guid>
		<description><![CDATA[Title of case study: To increase the Capacity of Machining. Project implementation start and end date: Jun-14 to Oct-14 Is it in continued operation now? Yes innovation: Elaborate in detail as to how your project stands out for its uniqueness...]]></description>
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		</div> 
	</div> <span style="color: #3572ad;"><strong>Title of case study:</strong></span><br />
To increase the Capacity of Machining.</p>
<p><span style="color: #3572ad;"><strong>Project implementation start and end date:</strong></span><br />
Jun-14 to Oct-14<br />
<span style="color: #3572ad;"><strong>Is it in continued operation now?</strong></span> Yes</p>
<p><span style="color: #3572ad;"><strong>innovation: Elaborate in detail as to how your project stands out for its uniqueness / innovation </strong></span></p>
<p>Following are the important, noticeable, unique &amp; innovative points of our project:/</p>
<ul style="margin-left: 60px;">1)Cycle time reduction in the existing processes without investment</ul>
<ul style="margin-left: 60px;">2)New wood pecking cycle designed &amp; implemented.</ul>
<ul style="margin-left: 60px;">3)Utilization of the idle machines by doing modification in fixture, tools, PLC program.</ul>
<ul style="margin-left: 60px;">4)Combination of the tool &amp; operation clubbing.</ul>
<ul style="margin-left: 60px;">5)All the activity has been carried out In-house &amp; lesser time.</ul>
<ul style="margin-left: 60px;">6)89% capacity up through this project within 3 months with minimum investment.</ul>
<p><span style="color: #3572ad;"><strong>Problem identification: Why was this problem selected? What methodology was adopted to identify the problem? </strong></span></p>
<p>We have selected this project due to following issues &amp; causes:-</p>
<ul style="margin-left: 60px;">1)Increasing trend in the customer requirement – capacity was short against the increasing requirement.</ul>
<ul style="margin-left: 60px;">2)It was not possible to fulfill the requirement by doing extra working also – OT cost is also high &amp; it cannot be solution for long term.</ul>
<ul style="margin-left: 60px;">3)Very less time to increase the capacity to fulfill customer requirement – lead time required for new line addition is more.</ul>
<ul style="margin-left: 60px;">4)High investment required for new line addition.</ul>
<ul style="margin-left: 60px;">5)Additional manpower requirement for new line.</ul>
<ul style="margin-left: 60px;">6)Additional space requirement for new line</ul>
<p>Our company’s market share is 70% with the higher level of satisfaction of the customers on account of QCDDM for which almost every year we have received an award. We are always giving the priority to the fulfillment of customer requirement.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/113.bmp"><img class="alignnone size-full wp-image-1759" src="https://productivity.imtma.in/wp-content/uploads/2016/09/113.bmp" alt="1" width="521" height="164" /></a></center>List of the causes affecting the cycle time :-</p>
<ul style="margin-left: 30px;">1)Wastage of non-cutting time.</ul>
<ul style="margin-left: 30px;">2)Idle machinery.</ul>
<ul style="margin-left: 30px;">3)Operations are in series.</ul>
<ul style="margin-left: 30px;">4)Process designed with the lower cutting speed.</ul>
<ul style="margin-left: 30px;">5)Delays due to errors in program.</ul>
<p>We have used various problem solving tools &amp; techniques for the problem identification as well as for root cause analysis:-</p>
<ul style="margin-left: 40px;">1)Brainstorming</ul>
<ul style="margin-left: 40px;">2)Data collection &amp; compilation.</ul>
<ul style="margin-left: 40px;">3)Pareto diagram.</ul>
<ul style="margin-left: 40px;">4)GEMBA / Situation Analysis.</ul>
<ul style="margin-left: 40px;">5)Cause &amp; effect diagram.</ul>
<ul style="margin-left: 40px;">6)5W1H</ul>
<ul style="margin-left: 40px;">7)Why-Why Analysis.</ul>
<ul style="margin-left: 40px;">8)PDCA.</ul>
<ul style="margin-left: 40px;">9)Run chart.</ul>
<ul style="margin-left: 40px;">10)Process capability study.</ul>
<ul style="margin-left: 40px;">11)Radar diagram.</ul>
<p>There was scope for:-</p>
<ul style="margin-left: 40px;">1)Improvement in the above mentioned causes in line with the CT reduction / Capacity increase.</ul>
<ul style="margin-left: 40px;">2)It can be done with minimum investment.</ul>
<ul style="margin-left: 40px;">3)It can be done faster OR in line with the customer requirement.</ul>
<ul style="margin-left: 40px;">4)It will have the better as well long term benefits to the organization.</ul>
<p><span style="color: #3572ad;"><strong>Data collection: What data was collected? What methodology was adopted to collect the data? </strong></span></p>
<p>In our project of capacity improvement we have collected, compiled &amp; analyzed following data:-</p>
<ul style="margin-left: 60px;">1)Objective trend.</ul>
<ul style="margin-left: 60px;">2)Machine wise, operation wise CT / time study.</ul>
<ul style="margin-left: 60px;">3)Process capability study.</ul>
<ul style="margin-left: 60px;">4)Technical data for the respective processes &amp; its parameters.</ul>
<ul style="margin-left: 60px;">5)Inspection data (diameter, depth, positions, angle, surface finish etc.)</ul>
<p>Usage of the e of the tools &amp; techniques for data collections:-</p>
<ul style="margin-left: 60px;">1)Data check sheet – used to collect the inspection data of the respective parameters.</ul>
<ul style="margin-left: 60px;">2)Run chart – used to understand the actual variation of the respective parameters.</ul>
<ul style="margin-left: 60px;">3)Time line chart – used to the time required for the respective activity in the respective process &amp; its impact on the CT.</ul>
<ul style="margin-left: 60px;">4)Process flow diagram – used to understand the sequence, relevance of each operation with each other.</ul>
<ul style="margin-left: 60px;">5)Job orientation study – used to identify the orientation of the job in case of the actual machining operations – for operation reshuffling &amp; clubbing.</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/25.bmp"><img class="alignnone size-full wp-image-1760" src="https://productivity.imtma.in/wp-content/uploads/2016/09/25.bmp" alt="2" width="390" height="163" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/33.bmp"><img class="alignnone size-full wp-image-1761" src="https://productivity.imtma.in/wp-content/uploads/2016/09/33.bmp" alt="3" width="425" height="164" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/42.bmp"><img class="alignnone size-full wp-image-1762" src="https://productivity.imtma.in/wp-content/uploads/2016/09/42.bmp" alt="4" width="392" height="251" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/53.bmp"><img class="alignnone size-full wp-image-1763" src="https://productivity.imtma.in/wp-content/uploads/2016/09/53.bmp" alt="5" width="325" height="252" /></a></center><span style="color: #3572ad;"><strong>Analysis and development of solution: What analysis was done? What alternate solutions were identified? Why was this particular solution chosen? </strong></span></p>
<ul>
<li>Brainstorming session was conducted to identify the various possible causes affecting the CT.</li>
<li>Machine wise, operation wise CT study has been done to identify the bottle neck machine as well as the bottleneck operation.</li>
<li>Operation wise, parameter wise, actual machining area / cutting area, non-cutting area, actual machine program has been studied to identify the various losses in the respective process / operations.</li>
<li>Standard technical data has been studied to check the existing process level &amp; scope for the corrections / improvements in the process parameters.</li>
<li>Job orientation &amp; operation feasibility review was conducted to check the possibility of doing the same operation on other machines (idle / underutilization mc).</li>
<li>Operation wise, activity wise time study is done to understand the most time consuming operation / activity.</li>
<li>Process flow diagram has been studied to know the sequence of the operations its importance &amp; the impacts</li>
<li>WHY-WHY analysis to identify the actual root cause of the problems.</li>
</ul>
<p><center><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/63.bmp"><img class="alignnone size-full wp-image-1764" src="https://productivity.imtma.in/wp-content/uploads/2016/09/63.bmp" alt="6" width="683" height="398" /></a></center></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/73.bmp"><img class="alignnone size-full wp-image-1765" src="https://productivity.imtma.in/wp-content/uploads/2016/09/73.bmp" alt="7" width="686" height="257" /></a></center><span style="color: #3572ad;"><strong>Implementation: How was the chosen solution tested/validated and implemented?</strong></span></p>
<p>Various data was studied, changes have been done in the respective parameters / program / operation location, sequence etc. &amp; accordingly trials have been conducted.<br />
Every step has been verified on account of the Quality inspection, safety, CT etc.<br />
Based on the inspection results decided to produce the trial lot &amp; verified up to the flow stand under the IP tag.<br />
Based on the final carburetor assembly results of flow stand &amp; after data compilation – standardization is done &amp; change point approval has been taken as per ‘Production Condition Change Application’ procedure.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/83.bmp"><img class="alignnone size-full wp-image-1766" src="https://productivity.imtma.in/wp-content/uploads/2016/09/83.bmp" alt="8" width="615" height="462" /></a></center>During the analysis of the problem, root cause, trials, selection of the correct action &amp; its</p>
<p>implementation process /activity – we have learned a lot of improvement in the concerned peoples:-</p>
<ul style="margin-left: 80px;">1)Leadership.</ul>
<ul style="margin-left: 80px;">2)Team work.</ul>
<ul style="margin-left: 80px;">3)Problem solving approach.</ul>
<ul style="margin-left: 80px;">4)Technical ability.</ul>
<ul style="margin-left: 80px;">5)Improvement approach.</ul>
<ul style="margin-left: 80px;">6)Computer skill, etc.</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/93.bmp"><img class="alignnone size-full wp-image-1767" src="https://productivity.imtma.in/wp-content/uploads/2016/09/93.bmp" alt="9" width="445" height="284" /></a></center><span style="color: #3572ad;"><strong>Benefits to organization: </strong></span><br />
<span style="color: #3572ad;"><strong>a)Operational benefits: What benefits were accrued to the organization as a result of the implementation of the project? </strong></span></p>
<p>Please list at least 4 important operational benefits on the parameters related to productivity, quality, etc. as relevant to this project.<br />
Following are the direct benefits from the project:-</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/102.bmp"><img class="alignnone size-full wp-image-1768" src="https://productivity.imtma.in/wp-content/uploads/2016/09/102.bmp" alt="10" width="694" height="132" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/114.bmp"><img class="alignnone size-full wp-image-1769" src="https://productivity.imtma.in/wp-content/uploads/2016/09/114.bmp" alt="11" width="693" height="295" /></a></center><span style="color: #3572ad;"><strong>b)Financial benefits: Describe the financial benefits on parameters such as cost saving, avoidance of CAPEX, etc. as relevant to this project.</strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/122.bmp"><img class="alignnone size-full wp-image-1770" src="https://productivity.imtma.in/wp-content/uploads/2016/09/122.bmp" alt="12" width="522" height="192" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/142.bmp"><img class="alignnone size-full wp-image-1771" src="https://productivity.imtma.in/wp-content/uploads/2016/09/142.bmp" alt="14" width="306" height="182" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/152.bmp"><img class="alignnone size-full wp-image-1772" src="https://productivity.imtma.in/wp-content/uploads/2016/09/152.bmp" alt="15" width="306" height="182" /></a></center><span style="color: #3572ad;"><strong>Institutionalization and horizontal deployment, if any:</strong></span></p>
<p>Please elaborate on how the changes have been embedded in the system and horizontally deployed as applicable.<br />
Horizontal deployment in all 3 plants of Keihinfie Pvt. Ltd. On PB as well as CV machining lines.</p>
<p>Contestants may give any other relevant information that can prove helpful to make it a winning entry.</p>
<ul>
<li>Some of the countermeasure (changes in the process parameters like speed, wood pecking cycle) also implemented on all the machining areas – Tool life also increased.</li>
<li>Our project is has been appreciated in the Keihinfie Quality Circle competition &amp; Winner of the year.</li>
<li>We have implemented the actions after thorough analysis, trials &amp; by following the standards of change point implementation procedure.</li>
<li>All the activities done very fast – as our target was to improve the capacity in line rather before customer requirement increase.</li>
</ul>
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		<title>SKF INDIA LIMITED PUNE</title>
		<link>https://productivity.imtma.in/skf-india-limited-pune/</link>
		<comments>https://productivity.imtma.in/skf-india-limited-pune/#comments</comments>
		<pubDate>Tue, 20 Sep 2016 06:38:38 +0000</pubDate>
		<dc:creator><![CDATA[Abhishek D]]></dc:creator>
				<category><![CDATA[2015]]></category>
		<category><![CDATA[Uncategorized]]></category>

		<guid isPermaLink="false">http://www.productivity.imtma.in/?p=1756</guid>
		<description><![CDATA[Title of case study: “Productivity Improvement at Channel Group 1 from 7000 Bearings/Day to 12000 Bearings/Day for two bearings types” Project implementation start and end date: Is it in continued operation now? Yes Innovation: Elaborate in detail as to how...]]></description>
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		</div> 
	</div> <span style="color: #3572ad;"><strong>Title of case study:</strong></span><br />
“Productivity Improvement at Channel Group 1 from 7000 Bearings/Day to 12000 Bearings/Day for two bearings types”</p>
<p><span style="color: #3572ad;"><strong>Project implementation start and end date:</strong></span></p>
<p><span style="color: #3572ad;"><strong>Is it in continued operation now?</strong></span> Yes</p>
<p><span style="color: #3572ad;"><strong>Innovation: Elaborate in detail as to how your project stands out for its uniqueness / innovation </strong></span></p>
<p><span style="color: #3572ad;"><strong>A] Consistent achievement of greater than 30% cost saved for 2 product types </strong></span></p>
<ul style="margin-left: 30px;">1.Without any investments in infrastructure.</ul>
<ul style="margin-left: 30px;">2.Without any direct material cost reduction.</ul>
<p><span style="color: #3572ad;"><strong>B] Both product types have already registered higher sales </strong></span></p>
<ul style="margin-left: 30px;">1.Product type 1 sale increased by 60% in volume</ul>
<ul style="margin-left: 30px;">2.Product type 2 sale increased by 60% in volume</ul>
<p><span style="color: #3572ad;"><strong>C] Additional capacity created leading to sales growth</strong></span></p>
<ul style="margin-left: 30px;">1.Both Product type sale increased to 45 k per month.</ul>
<p><span style="color: #3572ad;"><strong> D] Process Innovations </strong></span></p>
<ul style="margin-left: 30px;">1.Standardization for the process of Holistic cost reduction that can be replicated across SKF Globally</ul>
<ul style="margin-left: 30px;">2.Development of innovative process steps for improving performance of machines</ul>
<ul style="margin-left: 30px;">3.Process innovations like kinetic energy transformation DOE for grinding</ul>
<ul style="margin-left: 30px;">4.Process innovations like kinetic energy transformation honing process parameters.</ul>
<ul style="margin-left: 30px;">5.Sequential analysis for vibration scrap reduction</ul>
<ul style="margin-left: 30px;">6.Simulation DOE</ul>
<p><span style="color: #3572ad;"><strong>E] Sustainability </strong></span></p>
<ul style="margin-left: 30px;">1.Reduction in energy loss in grinding and honing by utilizing innovation idea of kinetic energy transformations</ul>
<ul style="margin-left: 30px;">2.Setup chart validated and incorporated in PLC and parameters lock to reduce man machine intervention.</ul>
<ul style="margin-left: 30px;">3.Training to all concerned employees completed across channels</ul>
<p><span style="color: #3572ad;"><strong> Problem identification: Why was this problem selected?<br />
What methodology was adopted to identify the problem? </strong></span></p>
<ul style="margin-left: 30px;">1.Business Threat of 20 MINR</ul>
<ul style="margin-left: 30px;">2.Selling Price of Bearing type 1 was 99.34 INR ,Standard cost of bearing was 100.88 INR, Actual Manufacturing cost was 148.8 INR, Competition was capturing market share for this type due to cost and capacity threat to the tune 1,00,000 brgs per year 10 MINR per year .</ul>
<ul style="margin-left: 30px;">3.Selling Price of Bearing type 2 was 98.55 INR ,Standard cost of bearing was105.09 INR, Actual Manufacturing cost was 124.8 INR, Competition was capturing market share for this type due to cost and capacity threat to the tune 1,00,000 brgs per year 10 MINR per year .</ul>
<ul style="margin-left: 30px;">4.Low productivity leading to Non Profitable business &amp; Loss to channel financial parameters</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/162.bmp"><img class="alignnone size-full wp-image-1776" src="https://productivity.imtma.in/wp-content/uploads/2016/09/162.bmp" alt="16" width="558" height="389" /></a></center><span style="color: #3572ad;"><strong> Business Excellence Approach </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/172.bmp"><img class="alignnone size-full wp-image-1777" src="https://productivity.imtma.in/wp-content/uploads/2016/09/172.bmp" alt="17" width="385" height="184" /></a></center><span style="color: #3572ad;"><strong> Data collection: What data was collected? What methodology was adopted to collect the data? </strong></span></p>
<p>1.Roadmap for productivity improvement &amp; cost reduction started with Structured approach of Standard Cost Break up from Cost controller .</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/182.bmp"><img class="alignnone size-full wp-image-1778" src="https://productivity.imtma.in/wp-content/uploads/2016/09/182.bmp" alt="18" width="533" height="193" /></a></center>2.Primary data for Baseline Efficiency and Output k/day for last 12 months was taken from Manufacturing channel to understand current productivity</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/192.bmp"><img class="alignnone size-full wp-image-1779" src="https://productivity.imtma.in/wp-content/uploads/2016/09/192.bmp" alt="19" width="547" height="247" /></a></center>3.Sensitivity Analysis DOE done for identifying contribution/impact of Individual Cost breakup parameters toward solving the problem</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/202.bmp"><img class="alignnone size-full wp-image-1780" src="https://productivity.imtma.in/wp-content/uploads/2016/09/202.bmp" alt="20" width="547" height="300" /></a></center><span style="color: #3572ad;"><strong> Analysis and development of solution: What analysis was done? What alternate solutions were identified? Why was this particular solution chosen? </strong></span></p>
<p>1.From Data collection and sensitive analysis 6 critical components were identified for further improvement An Integrated project management system with structured approach involving all channel management was used to ensuring timely completion of project activities</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/212.bmp"><img class="alignnone size-full wp-image-1781" src="https://productivity.imtma.in/wp-content/uploads/2016/09/212.bmp" alt="21" width="411" height="211" /></a></center>2.For Cycle and efficiency improvement …<br />
Use of Simulation tool for futuristic bottleneck discoveries coupled with Zero Loss study analytical tool with real time study to identify Cycle time loss machine ,Stoppages , Hidden output losses</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/222.bmp"><img class="alignnone size-full wp-image-1782" src="https://productivity.imtma.in/wp-content/uploads/2016/09/222.bmp" alt="22" width="342" height="164" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/231.bmp"><img class="alignnone size-full wp-image-1783" src="https://productivity.imtma.in/wp-content/uploads/2016/09/231.bmp" alt="23" width="328" height="166" /></a></center>3.For Efficiency loss –To reduce Scrap loss</p>
<ul>
<li>Analytical Technique of Sequential analysis for improving quality of bearings developed and deployed involving operators</li>
<li>This is very effective tool which builds a strong cause and effect relationship and contribution of each signification cause to effect via regression</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/241.bmp"><img class="alignnone size-full wp-image-1784" src="https://productivity.imtma.in/wp-content/uploads/2016/09/241.bmp" alt="24" width="347" height="185" /></a></center>4.Technique of optimizing grinding process based on kinetic energy transformation in process.(Design of Experiment)</p>
<p>5.Technique of optimizing honing parameters based on kinetic energy transformation and RSM (DOE)</p>
<p><span style="color: #3572ad;"><strong> Implementation: How was the chosen solution tested/validated and implemented? </strong></span></p>
<p><span style="color: #3572ad;"><strong> A} FIRST CRITICAL X ….OVERHEAD COST REDUCTION:</strong></span></p>
<p>Detail analysis was done categorically to understand Overhead cost parameters and which are important as seen in Pareto .</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/251.bmp"><img class="alignnone size-full wp-image-1785" src="https://productivity.imtma.in/wp-content/uploads/2016/09/251.bmp" alt="25" width="238" height="144" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/26.bmp"><img class="alignnone size-full wp-image-1786" src="https://productivity.imtma.in/wp-content/uploads/2016/09/26.bmp" alt="26" width="225" height="143" /></a></center><span style="color: #3572ad;"><strong> A1} WAGES </strong></span></p>
<p>As Per Pareto first priority was to analyse and reduce wages cost ,Wages was analysed in terms of no of fix workmen and flexi workmen and their actual reporting channel ,Allocation of workmen was done on basis of their actual working channel .Possibility of Reduction of manpower was seen as per value addition and recommendation was given.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/27.bmp"><img class="alignnone size-full wp-image-1787" src="https://productivity.imtma.in/wp-content/uploads/2016/09/27.bmp" alt="27" width="332" height="111" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/28.bmp"><img class="alignnone size-full wp-image-1788" src="https://productivity.imtma.in/wp-content/uploads/2016/09/28.bmp" alt="28" width="159" height="62" /></a></center><span style="color: #3572ad;"><strong> A2} COST DEPRICIATION </strong></span></p>
<p>Second Priority was Cost of Depreciation. Assets on Channel having written down value were verified for their availability on channel and were keened machine wise item wise and removed from asset register or reallocated to appropriate</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/29.bmp"><img class="alignnone size-full wp-image-1790" src="https://productivity.imtma.in/wp-content/uploads/2016/09/29.bmp" alt="29" width="231" height="175" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/30.bmp"><img class="alignnone size-full wp-image-1793" src="https://productivity.imtma.in/wp-content/uploads/2016/09/30.bmp" alt="30" width="169" height="111" /></a></center>channel</p>
<p>A} FINAL OVERHEAD COST REDUCTION After Analysis and action of overhead key parameter results show reduction in overhead cost</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/311.bmp"><img class="alignnone size-full wp-image-1794" src="https://productivity.imtma.in/wp-content/uploads/2016/09/311.bmp" alt="31" width="228" height="142" /></a></center>B} SECOND CRITICAL X ….Cycle time Reduction:</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/321.bmp"><img class="alignnone size-full wp-image-1795" src="https://productivity.imtma.in/wp-content/uploads/2016/09/321.bmp" alt="32" width="304" height="167" /></a></center>B1)Below is first Bottleneck machine ..SGB Inner ring groove grinding machine</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/331.bmp"><img class="alignnone size-full wp-image-1797" src="https://productivity.imtma.in/wp-content/uploads/2016/09/331.bmp" alt="33" width="270" height="196" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/34.bmp"><img class="alignnone size-full wp-image-1798" src="https://productivity.imtma.in/wp-content/uploads/2016/09/34.bmp" alt="34" width="159" height="130" /></a></center>B2) Then Second bottleneck was taken for complete study and DOE for optimization<br />
SHG IR Bore grinding machine</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/35.bmp"><img class="alignnone size-full wp-image-1800" src="https://productivity.imtma.in/wp-content/uploads/2016/09/35.bmp" alt="35" width="295" height="213" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/36.bmp"><img class="alignnone size-full wp-image-1801" src="https://productivity.imtma.in/wp-content/uploads/2016/09/36.bmp" alt="36" width="160" height="130" /></a></center>B3 )Then Third bottleneck was taken for complete study and DOE for optimization<br />
SSB Outer ring groove grinding machine</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/37.bmp"><img class="alignnone size-full wp-image-1802" src="https://productivity.imtma.in/wp-content/uploads/2016/09/37.bmp" alt="37" width="310" height="221" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/38.bmp"><img class="alignnone size-full wp-image-1804" src="https://productivity.imtma.in/wp-content/uploads/2016/09/38.bmp" alt="38" width="178" height="153" /></a></center>C} THIRD CRITICAL X --- EFFICIECNCY IMPROVEMENT</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/39.bmp"><img class="alignnone size-full wp-image-1806" src="https://productivity.imtma.in/wp-content/uploads/2016/09/39.bmp" alt="39" width="304" height="139" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/40.bmp"><img class="alignnone size-full wp-image-1807" src="https://productivity.imtma.in/wp-content/uploads/2016/09/40.bmp" alt="40" width="199" height="153" /></a></center>C1) SPC Inner ring face grinding machine defect was understood ..Glazing on face and detail causal analysis was done to identify root cause ..one of important aspect was Machine geometry which was checked and rectified during project activities .<br />
After Geometric alignment of machine Complete Kinetic Energy DOE was conducted for Feed position factors optimization ,Feed rate Factor optimizations and RSM DOE for Dressing parameter optimizations</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/411.bmp"><img class="alignnone size-full wp-image-1808" src="https://productivity.imtma.in/wp-content/uploads/2016/09/411.bmp" alt="41" width="285" height="202" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/43.bmp"><img class="alignnone size-full wp-image-1809" src="https://productivity.imtma.in/wp-content/uploads/2016/09/43.bmp" alt="43" width="188" height="173" /></a></center>C3 ) Outer Ring quality problem<br />
After Detail analysis ..Grinding allowance and Groove Radius allowance was found to be important parameter affecting wheel quality and ring quality ..<br />
Grinding allowance &amp; Radius modified and rings as per new drawing were procured for trials</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/44.bmp"><img class="alignnone size-full wp-image-1810" src="https://productivity.imtma.in/wp-content/uploads/2016/09/44.bmp" alt="44" width="289" height="215" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/45.bmp"><img class="alignnone size-full wp-image-1811" src="https://productivity.imtma.in/wp-content/uploads/2016/09/45.bmp" alt="45" width="188" height="59" /></a></center>C3) Outer ring Quality at FSF Honing machine was also optimized using Taguchi DOE with 7 Factors at 2 levels</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/46.bmp"><img class="alignnone size-full wp-image-1812" src="https://productivity.imtma.in/wp-content/uploads/2016/09/46.bmp" alt="46" width="230" height="164" /></a><br />
<a href="https://productivity.imtma.in/wp-content/uploads/2016/09/47.bmp"><img class="alignnone size-full wp-image-1813" src="https://productivity.imtma.in/wp-content/uploads/2016/09/47.bmp" alt="47" width="188" height="59" /></a></center><span style="color: #3572ad;"><strong> Benefits to organization: </strong></span><br />
<span style="color: #3572ad;"><strong>a) Operational benefits: </strong></span></p>
<div class="new_pro_tbl">
<table>
<tbody>
<tr>
<td ><strong><b>Sr No</b></strong></td>
<td ><strong><b>Parameter</b></strong></td>
<td ><strong><b>Benefit</b></strong></td>
</tr>
<tr>
<td rowspan="3" ><strong><b>1</b></strong></td>
<td rowspan="3" ><strong><b> </b></strong><strong><b>Productivity</b></strong></p>
<p><strong><b> </b></strong></td>
<td ><strong><b>Channel productivity improvement for two types from 7000 bearings/day to 12000 bearings/ day</b></strong></td>
</tr>
<tr>
<td ><strong><b> Cycle time reduced from 9 sec to 5.4 sec</b></strong></td>
</tr>
<tr>
<td ><strong><b>Sales increased from 28000 to 45000 bearings/month for both types</b></strong></td>
</tr>
<tr>
<td ><strong><b>2</b></strong></td>
<td><strong><b>Machine Availability</b></strong></td>
<td><b>· </b><strong><b>Machine Adjustment and stoppages reduced from 4% to 1% </b></strong><b>· </b><strong><b>Spindle Failures eliminated </b></strong></td>
</tr>
<tr>
<td rowspan="4" ><strong><b>3</b></strong></td>
<td rowspan="4" ><strong><b>Quality</b></strong><strong><b> </b></strong></td>
<td ><strong><b>Vibration Scrap reduced from 10% to 2%</b></strong></td>
</tr>
<tr>
<td ><strong><b>Bore scrap reduced from 3% to 0.5%</b></strong></td>
</tr>
<tr>
<td ><strong><b>Pairing capability improved</b></strong></td>
</tr>
<tr>
<td ><strong><b>First time yield improved from 90 to 98%</b></strong></td>
</tr>
<tr>
<td ><strong><b>4</b></strong></td>
<td ><strong><b>Safety</b></strong></td>
<td ><strong><b>Operator fatigue reduced </b></strong></td>
</tr>
<tr>
<td ><strong><b>5</b></strong></td>
<td ><strong><b>Morale</b></strong></td>
<td >
<ul>
<li><strong><b>Complete involvement from top management to all employees involved in project with numerous knowledge sharing sessions.</b></strong> </li>
<li><strong><b>Active Involvement of all Employees in complete process</b></strong></li>
<li> <strong><b>Project Appreciate by SKF Group Top Management</b></strong></li>
<p> <a href="https://productivity.imtma.in/wp-content/uploads/2016/09/48.bmp"><img class="alignnone size-full wp-image-1815" src="https://productivity.imtma.in/wp-content/uploads/2016/09/48.bmp" alt="48" width="219" height="164" /></a></td>
</tr>
</tbody>
</table>
</div>
<p><span style="color: #3572ad;"><strong> b)Financial benefits: </strong></span></p>
<div class="new_pro_tbl">
<table>
<tbody>
<tr>
<td ><strong><b>Sr No</b></strong></td>
<td ><strong><b>Parameter</b></strong></td>
<td ><strong><b>Benefit</b></strong></td>
</tr>
<tr>
<td ><strong><b>1</b></strong></td>
<td ><strong><b>Cost</b></strong></td>
<td ><strong><b>Cost per bearing reduced from 148.8 Rs to 98.3 Rs</b></strong></td>
</tr>
<tr>
<td ><strong><b>2</b></strong></td>
<td ><strong><b>Profitability</b></strong></td>
<td ><strong><b>Financial benefits to organization 23,000,000 Rs./annum</b></strong></td>
</tr>
</tbody>
</table>
</div>
<p><span style="color: #3572ad;"><strong> Institutionalization and horizontal deployment, if any: </strong></span></p>
<p>Please elaborate on how the changes have been embedded in the system and horizontally deployed as applicable.<br />
Umbrella Project Launched Across Channels of DGBB Pune on Different channels as per Customer Threat and Business Volume</p>
<p>&nbsp;</p>
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		<title>Bajaj Auto Ltd</title>
		<link>https://productivity.imtma.in/bajaj-auto-ltd-2/</link>
		<comments>https://productivity.imtma.in/bajaj-auto-ltd-2/#comments</comments>
		<pubDate>Mon, 19 Sep 2016 09:50:36 +0000</pubDate>
		<dc:creator><![CDATA[Abhishek D]]></dc:creator>
				<category><![CDATA[2015]]></category>

		<guid isPermaLink="false">http://www.productivity.imtma.in/?p=1700</guid>
		<description><![CDATA[Title of case study: Maximize overall equipment efficiency for Capacity enhancement with minimal capital investment. Project implementation start and end date: Aug 2012 to Jan, 2013 Is it in continued operation now? Yes Certificate of the division/business/unit/company head We certify...]]></description>
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	<div class="vc_col-sm-12 wpb_column clr column_container  ">
			
	</div> 

	<div class="wpb_text_column wpb_content_element ">
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		</div> 
	</div> <span style="color: #3572ad;"><strong>Title of case study:</strong></span><br />
Maximize overall equipment efficiency for Capacity enhancement with minimal capital investment.</p>
<p><span style="color: #3572ad;"><strong>Project implementation start and end date:</strong></span><br />
Aug 2012 to Jan, 2013</p>
<p><span style="color: #3572ad;"><strong>Is it in continued operation now?</strong></span> Yes</p>
<p><span style="color: #3572ad;"><strong>Certificate of the division/business/unit/company head</strong></span></p>
<ul>
<li>We certify that the productivity improvement project described here was implemented by the above team and is in continuous operation. We also certify that the claimed benefits accrued to our organization. We also agree that the contents of this case study can be published by the organizers.</li>
</ul>
<p><span style="color: #3572ad; margin-left: 40px;"><strong> Innovation / Uniqueness: </strong></span></p>
<ul>
<li>Every business is for making profit. Loss in profit loss or sales loss is not acceptable in any company at any circumstances. Our project has addressed the same objective.</li>
<li>As chassis shop is governing the entire plants output, if the required capacity could not have achieved, we could have lost vehicle sales (including exports) to the tune of 10 to 12 K per month, resulting direct loss of profit to company.</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/11.bmp"><img class="alignnone size-full wp-image-1703" src="https://productivity.imtma.in/wp-content/uploads/2016/09/11.bmp" alt="1" width="416" height="265" /></a></center></p>
<ul>
<li>We studied this project TPM way with micro level and deeply working to identify small small possible contributing elements of cycle time reduction.</li>
<li>Systematic analysis is done through management tools e.g. tree diagram, possibility matrix, ECRS &amp; time motion micro study. We struggled for saving even 0.1 sec / spot &amp; achieved through RW software by interfacing with machine manufacturer &amp; learning on internet. 0.1 sec/spot reductions resulted into 15.4 sec. saving on 14 Robots.</li>
<li>We believe in team working, our team has complemented the challenging project successfully. Our satisfied team consists of cell members, group leaders, managers &amp; divisional head.</li>
<li>Our teams working at ‘Gemba’ demonstrated the true implementation of Japanese concept of small improvements (Kaizen) gives big results in this project.</li>
</ul>
<p><span style="color: #3572ad;"><strong>Problem identification: </strong></span></p>
<p>Bajaj Auto’s 3Wheelers passengers are having dominant presence in both Domestic as well as Export market. In last 3-4 years, Bajaj was facing stiff competition from other manufacturers to retain its market leadership. Also, customer expectations are increasing w.r.t. mileage, durability &amp; comfort. While supplying good reliable products to our customers, our aim is to reduce on the operating costs and enhance the required capacities with minimal capital investments. With this lean approach Bajaj Auto is industry leader &amp; distinctly ahead in terms of its EBITDA margins.<br />
To take on the competition, Bajaj Auto decided to upgrade the entire range of its 3 Wheelers and launched new series of models under the Facelift category. In new model chassis, the no. of spots increased from 186 to 217 nos., increasing the robotic welding line cycle time from 42 to 52.6 sec. Due to this, the capacity dropped from 50 K to 40 K per month.<br />
As chassis shop is governing the entire plants output, if the required capacity could not have achieved, we could have lost vehicle sales (including exports) to the tune of 10 to 12 K per month, resulting direct loss of profit to company.<br />
Loss in profit is not at all acceptable; hence this project is selected to resolve on top most priority.<br />
To restore the cycle time, it was necessary to add minimum 2 Robots to accommodate the additional 31 spots and these 2 robots need to be added before the dash board welding stage. Though spotting time would have been addressed by adding 2 robots, it was calling for major change in the line layout which would have affected the entire cell layout with shifting of minimum 6 robots and modification of the chassis handling system &amp; it would require 15 days shutdown. Cost involved was Rs.126 Lacs. Considering the time &amp; cost involved, this option is beyond consideration.<br />
So we have taken challenge of cycle time reduction through TPM way deeply working.<br />
With deep analysis of cycle time (both Weld &amp; Non weld time) and implementing innovative Kaizens, the cycle time was restored to 42 sec in first phase and further reduced to 40 sec to meet the increased demand.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/21.bmp"><img class="alignnone size-full wp-image-1704" src="https://productivity.imtma.in/wp-content/uploads/2016/09/21.bmp" alt="2" width="419" height="130" /></a></center><br />
<span style="color: #3572ad;"><strong>Data collection: </strong></span></p>
<p>Elemental micro time study on Robotic line – chassis welding cell was conducted &amp; accurate data has been collected for each Robot &amp; transfer equipment. This data has been used to arrive at time for each operation, to prioritize, analyze and take necessary action to improve the capacity of Robotic welding line.<br />
We have scanned Robotic line for time &amp; motion study. Through which we have collected the data of time /spot, no of spots per Robot, Robot speed, Robot home position distance from chassis, line layout, Robot air cutting time &amp; welding time, process parameters for optimization. All this collected &amp; taken for analysis &amp; corrective measures.</p>
<p><span style="color: #3572ad;"><strong>Cell Layout </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/31.bmp"><img class="alignnone size-full wp-image-1705" src="https://productivity.imtma.in/wp-content/uploads/2016/09/31.bmp" alt="3" width="650" height="154" /></a></center><br />
<span style="color: #3572ad;"><strong>Robot wise spot distribution</strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/4.bmp"><img class="alignnone size-full wp-image-1706" src="https://productivity.imtma.in/wp-content/uploads/2016/09/4.bmp" alt="4" width="500" height="154" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/51.bmp"><img class="alignnone size-full wp-image-1707" src="https://productivity.imtma.in/wp-content/uploads/2016/09/51.bmp" alt="5" width="650" height="222" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/61.bmp"><img class="alignnone size-full wp-image-1708" src="https://productivity.imtma.in/wp-content/uploads/2016/09/61.bmp" alt="6" width="500" height="250" /></a></center><span style="color: #3572ad;"><strong>Analysis and development of solution: </strong></span></p>
<p>Robotic Line cycle time data has been analyzed through detailed elemental time study sheet and ECRS.<br />
Captured hidden losses - Motion loss, waiting time, delay were addressed through idea matrix management tool. Different ideas generated with the help of this idea matrix. Idea applicability matrix tool is used to identify the scope of each idea at different places. Why why analysis has been conducted to find the root cause to arrive a solutation. Ishikawa &amp; tree diagram tool was used to identify the different contributing factors for cycle time improvement.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/71.bmp"><img class="alignnone size-full wp-image-1711" src="https://productivity.imtma.in/wp-content/uploads/2016/09/71.bmp" alt="7" width="503" height="151" /></a></center><span style="color: #3572ad;"><strong>Idea Matrix </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/81.bmp"><img class="alignnone size-full wp-image-1712" src="https://productivity.imtma.in/wp-content/uploads/2016/09/81.bmp" alt="8" width="503" height="188" /></a></center><br />
<span style="color: #3572ad;"><strong>Idea Applicability Matrix </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/91.bmp"><img class="alignnone size-full wp-image-1713" src="https://productivity.imtma.in/wp-content/uploads/2016/09/91.bmp" alt="9" width="553" height="208" /></a></center><br />
<span style="color: #3572ad;"><strong>Tree Diagram </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/10.bmp"><img class="alignnone size-full wp-image-1714" src="https://productivity.imtma.in/wp-content/uploads/2016/09/10.bmp" alt="10" width="508" height="120" /></a></center><br />
<span style="color: #3572ad;"><strong>Implementation: </strong></span></p>
<p>We studied all the cycle time (both Weld time &amp; Non weld time i.e. handling time) for the entire line.<br />
We analysed the time required per spot and found that Robot takes total 7 steps to perform 1 spot and the time required is 2 Sec / spot.<br />
To reduce the time per spot, we adopted the “Spotware” software, due to which the time per spot can be reduced from 2 sec to 1.90 sec per spot. This reduction of 0.10 Sec per spot means total saving of @ 16 Sec for the total 217 spots in new model.<br />
The Robots interface control panels &amp; welding gun were modified to adopt the software and with saving of total 15.7 sec, 8 no. of spots were accommodated in the existing robots itself.<br />
Another 5 spots were accommodated by detail study of each robots utilization &amp; re-grouping of the spots and only one robot was added for balance spots.<br />
With this, we avoided the shifting of robots and the cycle time was restored by adding only 1 robot without any major change in the cell layout and handling system.<br />
Kaizen – Use ‘Spotware software’ to reduce time / spot</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/111.bmp"><img class="alignnone size-full wp-image-1715" src="https://productivity.imtma.in/wp-content/uploads/2016/09/111.bmp" alt="11" width="493" height="269" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/12.bmp"><img class="alignnone size-full wp-image-1716" src="https://productivity.imtma.in/wp-content/uploads/2016/09/12.bmp" alt="12" width="503" height="160" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/13.bmp"><img class="alignnone size-full wp-image-1717" src="https://productivity.imtma.in/wp-content/uploads/2016/09/13.bmp" alt="13" width="509" height="164" /></a></center>To reduce the cycle time from 42 Sec to 40 Sec, it required not only addition of 2 more Robots, but also major modification of the handling equipments for transferring the chassis from stage to stage on the welding line. It was challenge to reduce cycle time further without any new investment. With deep study by the team, the cause analysis concluded on 2 main aspects i.e. ‘Slow speed of dog chain conveyor’ (for chassis transfer) and ‘More waiting time for Robots as well as the pick &amp; place unit’ (for chassis handling).<br />
Example: Simultaneous movements of Pick &amp; Place unit &amp; indexing unit while Robot Spot welding</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/14.bmp"><img class="alignnone size-full wp-image-1718" src="https://productivity.imtma.in/wp-content/uploads/2016/09/14.bmp" alt="14" width="464" height="193" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/15.bmp"><img class="alignnone size-full wp-image-1719" src="https://productivity.imtma.in/wp-content/uploads/2016/09/15.bmp" alt="15" width="516" height="301" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/16.bmp"><img class="alignnone size-full wp-image-1720" src="https://productivity.imtma.in/wp-content/uploads/2016/09/16.bmp" alt="16" width="519" height="278" /></a></center><br />
<span style="color: #3572ad;"><strong>Benefits to organization: </strong></span><br />
<span style="color: #3572ad;"><strong>a)Operational benefits: </strong></span></p>
<ul>
<li>Cycle time restored and reduced from 52.6 sec to 40 sec.</li>
<li>Production per hour increased from 68 to 89 Nos.</li>
<li>Capacity Restoration to 50 K per month with New models and avoided sales loss.</li>
<li>Further cycle time reduction for Capacity enhancement to more than 52 K per month to cater the increased market demand.</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/17.bmp"><img class="alignnone size-full wp-image-1721" src="https://productivity.imtma.in/wp-content/uploads/2016/09/17.bmp" alt="17" width="420" height="128" /></a></center><br />
<span style="color: #3572ad;"><strong>b)Financial benefits: </strong></span></p>
<ul>
<li>Capacity Restoration to 50 K per month with New models with Investment Cost saving of Rs. 56 Lacs …. <b>No loss of production</b></li>
<li>Avoided addition of 2 Robots (Investment of Rs. 70 Lacs)</li>
<li><b>Total Investment cost saved : Rs. 126 lacs</b></li>
</ul>
<p><span style="color: #3572ad;"><strong>Institutionalization and horizontal deployment, if any: </strong></span></p>
<p>Chassis assembly Process sheet &amp; Input-Process-Output (IPO) modified in line with the changes made with the help of ME dept.<br />
Following documents are revised by adding the more check points to sustain the changes implemented.<br />
JH, PM, OPL &amp; SOP sheets updated, Process parameter document revised, Pick &amp; place, EMS drive values, parameters sheet revised, machine master list updated in the SAP system, machine manual of ABB robot, SPM, Pick &amp; place, EMS, Pallet conveyor, Tracks, lifters are modified with the help of central maintenance. Safety audit check sheet revised &amp; communicated to the central safety dept. Training of revised process is given to cell members &amp; concern managers &amp; respective data updated along with HR dept.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/18.bmp"><img class="alignnone size-full wp-image-1722" src="https://productivity.imtma.in/wp-content/uploads/2016/09/18.bmp" alt="18" width="404" height="215" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/19.bmp"><img class="alignnone size-full wp-image-1723" src="https://productivity.imtma.in/wp-content/uploads/2016/09/19.bmp" alt="19" width="403" height="215" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/20.bmp"><img class="alignnone size-full wp-image-1724" src="https://productivity.imtma.in/wp-content/uploads/2016/09/20.bmp" alt="20" width="406" height="216" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/211.bmp"><img class="alignnone size-full wp-image-1725" src="https://productivity.imtma.in/wp-content/uploads/2016/09/211.bmp" alt="21" width="403" height="216" /></a></center>All these learning and improvement have been applied on maxima Chassis Assly Robotic line which is already existing chassis shop 3Wh. We have also shared these learning with our vendors and suppliers (Business partners) who are having Robotic spot welding lines and implemented horizontally.<br />
Same learning is shared with ME, Purchase &amp; Engineering department for future procurement of Robots and equipments which will have same features so that benefit can get for the day one.</p>
<p><span style="color: #3572ad;"><strong>Other relevant information:</strong></span></p>
<ul>
<li>Executed the above project within the span of 6 months only with payback of 3 months.</li>
<li>Project is implemented by working on weekly offs without loss of production.</li>
<li>New model launched on time without any sales loss with sustained OEE, Zero defect &amp; Cost reduction.</li>
</ul>
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		<title>Lucas TVS Ltd</title>
		<link>https://productivity.imtma.in/ms-lucas-tvs-ltd/</link>
		<comments>https://productivity.imtma.in/ms-lucas-tvs-ltd/#comments</comments>
		<pubDate>Mon, 19 Sep 2016 08:59:22 +0000</pubDate>
		<dc:creator><![CDATA[Abhishek D]]></dc:creator>
				<category><![CDATA[2015]]></category>

		<guid isPermaLink="false">http://www.productivity.imtma.in/?p=1727</guid>
		<description><![CDATA[Title of case study: RAMP-UP OF SGM25 (Sundaram Gear Reduction Motor) Project implementation start and end date: 19.9.2014 to 26.11.2014 Is it in continued operation now? Yes Innovation: Elaborate in detail as to how your project stands out for its...]]></description>
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		</div> 
	</div> <span style="color: #3572ad;"><strong>Title of case study:</strong></span></p>
<p>RAMP-UP OF SGM25 (Sundaram Gear Reduction Motor)</p>
<p><span style="color: #3572ad;"><strong>Project implementation start and end date:</strong></span></p>
<p>19.9.2014 to 26.11.2014</p>
<p><span style="color: #3572ad;"><strong>Is it in continued operation now?</strong></span> Yes</p>
<p><span style="color: #3572ad; margin-left: 40px;"><strong>Innovation: Elaborate in detail as to how your project stands out for its uniqueness / innovation.</strong></span></p>
<ul>
<li>Sudden increase in customer demand for LD-GRS platform1.0 lit starter motor, needing augmentation of capacity by 2-times of the current level the capacity enhancement done by leveraging on the In-house experience, competency and talents. Innovative ideas implemented in all the key cells of the starter motor manufacturing value stream.</li>
</ul>
<p><b>Armature line improvements:</b></p>
<ul style="margin-left: 30px;">
<li>Plan and control to optimize flow in Armature manufacturing cell (Heijunka-leveled production) adopted (Result Armature line balancing output increased by 15%)</li>
<li>Innovative methods adopted in core pack lamination tool design to improve the input imbalance of the core pack and reduce the final rejection in Armature manufacturing (Result : Armature output increased by 30 % )</li>
<li>“MTTR” improved in armature manufacturing Dynamic balancing machine and conductor fusing machine by upgrading the control system (both hardware+software). (Result: Down time of both the machines were reduced &amp; MTTR improved from 45min to 3.2 min system up gradation also helped to reduce the cycle time by elimination of additional station(Audit station) in the operation sequence )</li>
<li>Cycle time reduction in one of the critical bottleneck stage armature core and commutator machining operation by upgrading the special cutting tools and re-design of tool layout.</li>
</ul>
<p><b>Yoke &amp; Sub-assembly line improvements:</b></p>
<ul style="margin-left: 30px;">
<li>SMED concept implemented in Yoke, Armature &amp; Sub-assemble manufacturing cell to minimize losses due to change over time (Armature line equipped with 80% one-off critical capital intensive machines )</li>
<li>Engineering solution arrived for final performance testing of starter motor to de-bottle necked (Result: Cycle time reduced 38 sec to 27sec.Hence output increase by 20%).</li>
</ul>
<p><span style="color: #3572ad;"><strong>Problem identification: Why was this problem selected? What methodology was adopted to identify the problem?</strong></span></p>
<p>Customer has come with sudden volume ramp-up increased by 100% in SGM25 starter motor assy from 800 no’s to 1600 no’s/day. But the current capacity was 1086 nos in Armature assembly which is the lowest capacity module among the all sub-assemblies.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/110.bmp"><img class="alignnone size-full wp-image-1730" src="https://productivity.imtma.in/wp-content/uploads/2016/09/110.bmp" alt="1" width="466" height="259" /></a></center><b>Tentative root causes:</b></p>
<ul style="margin-left: 30px;">
<li>Some of the Critical process in sub assemblies were identified as bottleneck stations</li>
<li>Down time and MTTR in Armature assembly is high</li>
<li>Product change over time is high in Armature assembly.</li>
<li>Imbalance rejection in Armature assy is high</li>
<li>Disruption of workflow in armature assy brown stage</li>
</ul>
<p><b>Tools and Techniques used:</b></p>
<ul style="margin-left: 200px;">
<li>TAKT time analysis – To identify bottleneck stations</li>
<li>Time study – Used stopwatch to take COT study</li>
<li>Bar graph – Imbalance rejection trend</li>
<li>Down time study and analysis – To reduce MTTR</li>
<li>HEIJUNKA - Flow line study</li>
</ul>
<p>Task force was formed to do productivity improvements in all modules to meet the customer demand with less investment in a short period of time</p>
<p><span style="color: #3572ad;"><strong>Data collection: What data was collected? What methodology was adopted to collect the data? </strong></span></p>
<p><center><b>“DEMAND CHART</b></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/22.bmp"><img class="alignnone size-full wp-image-1731" src="https://productivity.imtma.in/wp-content/uploads/2016/09/22.bmp" alt="2" width="521" height="198" /></a></center>&nbsp;</p>
<ul>
<li><b>Demand increase due to localization of starter motor &amp; new product volume increase in the market.</b></li>
</ul>
<p><span style="color: #3572ad;"><strong> Identification of process measures: </strong></span></p>
<p>We have done “TAKT” time analysis and time study for all sub assemblies &amp; main assemblies to identify the bottleneck station to do productivity improvements</p>
<p><span style="color: #3572ad;"><strong> Tools and Techniques. </strong></span></p>
<ul style="margin-left: 70px;">
<li>Takt Time study.</li>
<li>SMED and Cycle time study</li>
<li>Rejection trend analysis .</li>
<li>Downtime &amp; MTTR analysis in Armature balancing machine.</li>
</ul>
<p><span style="color: #3572ad;"><strong> Comprehensiveness of data collection: </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/32.bmp"><img class="alignnone size-full wp-image-1732" src="https://productivity.imtma.in/wp-content/uploads/2016/09/32.bmp" alt="3" width="522" height="123" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/41.bmp"><img class="alignnone size-full wp-image-1733" src="https://productivity.imtma.in/wp-content/uploads/2016/09/41.bmp" alt="4" width="457" height="178" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/52.bmp"><img class="alignnone size-full wp-image-1734" src="https://productivity.imtma.in/wp-content/uploads/2016/09/52.bmp" alt="5" width="435" height="176" /></a></center><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/62.bmp"><img class="alignnone size-full wp-image-1735" src="https://productivity.imtma.in/wp-content/uploads/2016/09/62.bmp" alt="6" width="450" height="183" /></a></center><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/72.bmp"><img class="alignnone size-full wp-image-1736" src="https://productivity.imtma.in/wp-content/uploads/2016/09/72.bmp" alt="7" width="416" height="152" /></a></center><span style="color: #3572ad;"><strong>Analysis and development of solution: What analysis was done? What alternate solutions were identified? Why was this particular solution chosen? </strong></span></p>
<ul style="margin-left: 70px;">
<li>We checked imbalance value in every stage and found not much variation. So we tried to reduce the initial imbalance of input component by restricting the sheet metal thickness variation and optimizing the pitch setting of lamination blanking tool</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/82.bmp"><img class="alignnone size-full wp-image-1737" src="https://productivity.imtma.in/wp-content/uploads/2016/09/82.bmp" alt="8" width="594" height="152" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/92.bmp"><img class="alignnone size-full wp-image-1738" src="https://productivity.imtma.in/wp-content/uploads/2016/09/92.bmp" alt="9" width="331" height="154" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/101.bmp"><img class="alignnone size-full wp-image-1739" src="https://productivity.imtma.in/wp-content/uploads/2016/09/101.bmp" alt="10" width="328" height="153" /></a></center></p>
<ul style="margin-left: 70px;">
<li>Reduction of both cutting &amp; non cutting time was planned in Core &amp; Commutator OD turning process. Peripheral activity timing was reduced (51 to 38 Sec) &amp; improved insert with sharper geometry was chosen to reduce double pass (38 to 30 Sec).</li>
<li>In output shaft bush and pin assy, while doing bush and pin pressing in single station auto loading of bush and indexing of tool takes more time. So we separated both operations</li>
<li>In performance test rig, 10 times cranking was done against the spec of 5 times for our product endurability. After having consistency in performance, we decided to reduce cranking cycles with approval of product Engineering and quality assurance.</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/112.bmp"><img class="alignnone size-full wp-image-1740" src="https://productivity.imtma.in/wp-content/uploads/2016/09/112.bmp" alt="11" width="558" height="154" /></a><center></center></center></p>
<ul style="margin-left: 70px;">
<li>Among the four underutilized machines, varnish plant was upgraded and the other three were tooled up to suit SGM25.</li>
<li>SMED - QCT tooling’s planned for Core assy, Conductor twisting and Radial insertion machines which are having more COT</li>
<li>Input imbalance of corepack was correlated with Face out and R/O and it was reduced by pitch setting. Commutator imbalance was reduced at supplier end by optimizing the process parameters in manufacturing. Where the rejected corepack and commutators were reworked and we can use it.</li>
<li>MTTR analysis – Balancing and Hotstaking m/c were selected to reduce MTTR .Introduced upgraded hardware unit in balancing m/c and pressure switch for ensuring the collet clamping in Hotstaking</li>
</ul>
<p><span style="color: #3572ad;"><strong>Implementation: How was the chosen solution tested/validated and implemented? </strong></span></p>
<p>(1) Developed sheet metal thickness variation within 5 microns was tried out to reduce face out of the component within 0.2 mm. We checked 1000 no’s for initial imbalance and found 98.45 % of the core pack are below 500 mg. The rejected corepack were reworked by machining the core OD to reduce CE, DE and Static imbalance.</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/121.bmp"><img class="alignnone size-full wp-image-1741" src="https://productivity.imtma.in/wp-content/uploads/2016/09/121.bmp" alt="12" width="401" height="106" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/131.bmp"><img class="alignnone size-full wp-image-1742" src="https://productivity.imtma.in/wp-content/uploads/2016/09/131.bmp" alt="13" width="402" height="106" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/141.bmp"><img class="alignnone size-full wp-image-1743" src="https://productivity.imtma.in/wp-content/uploads/2016/09/141.bmp" alt="14" width="511" height="159" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/151.bmp"><img class="alignnone size-full wp-image-1744" src="https://productivity.imtma.in/wp-content/uploads/2016/09/151.bmp" alt="15" width="518" height="171" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/161.bmp"><img class="alignnone size-full wp-image-1745" src="https://productivity.imtma.in/wp-content/uploads/2016/09/161.bmp" alt="16" width="418" height="142" /></a></center>In balancing, measuring station was upgraded with latest version to eliminate booting error and less response to the communication given to milling station.</p>
<p>In Hot staking, clamping of component feedback taken from proximity sensor. Due to ineffectiveness in sensing, interruptions were observed frequently.</p>
<p><span style="color: #3572ad;"><strong>SMED – QCT provided in three m/c and COT was reduced from 60min to10 min </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/171.bmp"><img class="alignnone size-full wp-image-1746" src="https://productivity.imtma.in/wp-content/uploads/2016/09/171.bmp" alt="17" width="571" height="121" /></a></center><span style="color: #3572ad;"><strong>Benefits to organization: </strong></span></p>
<p><span style="color: #3572ad;">Operational benefits: What benefits were accrued to the organization as a result of the implementation of the project? </span></p>
<ul>
<li>Customer satisfaction by enhancing the capacity from <b>800/day to 1600/day</b> in shortest possible lead time.</li>
<li>Support export market to realize a sales value grown up to<b> Rs66.0 lakhs/month </b>(New business)</li>
<li>Savings Thro’ productivity improvements; 30 % Increased</li>
</ul>
<ul style="margin-left: 50px;">
<li>a.Manpower reduction 15 man .(optimize the armature flow line improvement done ,Cycle time reduction (core OD turning, Conductor fusing and Performance testing )</li>
<li>b.SMED Applied ,Setting change over reduction doneTools investment cost / consumables cost reduction.</li>
</ul>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/181.bmp"><img class="alignnone size-full wp-image-1747" src="https://productivity.imtma.in/wp-content/uploads/2016/09/181.bmp" alt="18" width="560" height="137" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/191.bmp"><img class="alignnone size-full wp-image-1748" src="https://productivity.imtma.in/wp-content/uploads/2016/09/191.bmp" alt="19" width="548" height="186" /></a></center><span style="color: #3572ad;"><strong>b)Financial benefits: Describe the financial benefits on parameters such as cost saving, avoidance of CAPEX, etc. as relevant to this project. </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/201.bmp"><img class="alignnone size-full wp-image-1749" src="https://productivity.imtma.in/wp-content/uploads/2016/09/201.bmp" alt="20" width="539" height="236" /></a></center>&nbsp;</p>
<p>Institutionalization and horizontal deployment, if any:</p>
<p>Please elaborate on how the changes have been embedded in the system and horizontally deployed as applicable</p>
<p><span style="color: #3572ad;"><strong> Standardization: </strong></span></p>
<p>(a). Process change note(PCN) raised for cycle time reduction in core &amp; commutator OD turning and got approved from Quality Manager – Form no.</p>
<p>(b) SOP provided for checking of Core and Commutator imbalance checking and also for reuse of rejected core pack and Commutator after reducing initial imbalance by doing rework.</p>
<p>(c) Component approval made for major tooling, process change and re-establishment of process in underutilized machines – Form no</p>
<p>(d) All the improvements done in this project have been standardized through KAIZEN sheet.</p>
<p><span style="color: #3572ad;"><strong> Horizontal deployment: </strong></span></p>
<p>(a). Same idea in reducing the initial imbalance has been adopted in other varieties like M70 – PRD3, M74 and M70s LTV and successfully we have improved the productivity .</p>
<p>(b) Cycle time reduction in core OD turning process has been going on for the following machines IA0061, IA0049 &amp; IA0057</p>
<p><span style="color: #3572ad;"><strong> Contestants may give any other relevant information that can prove helpful to make it a winning entry. </strong></span></p>
<p><span style="color: #3572ad;"><strong> Lamination blanking tool </strong></span></p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/221.bmp"><img class="alignnone size-full wp-image-1750" src="https://productivity.imtma.in/wp-content/uploads/2016/09/221.bmp" alt="22" width="400" height="142" /></a></center>&nbsp;</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/23.bmp"><img class="alignnone size-full wp-image-1751" src="https://productivity.imtma.in/wp-content/uploads/2016/09/23.bmp" alt="23" width="422" height="153" /></a></center>SOP for checking core pack imbalance and reuse of high imbalanced commutator</p>
<p><center><a href="https://productivity.imtma.in/wp-content/uploads/2016/09/24.bmp"><img class="alignnone size-full wp-image-1752" src="https://productivity.imtma.in/wp-content/uploads/2016/09/24.bmp" alt="24" width="565" height="168" /></a></center></p>
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