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	<title>Productivity Portal &#187; 2014</title>
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		<title>Maruti Suzuki India Ltd</title>
		<link>https://productivity.imtma.in/maruti-suzuki-india-ltd/</link>
		<comments>https://productivity.imtma.in/maruti-suzuki-india-ltd/#comments</comments>
		<pubDate>Tue, 20 Jan 2015 14:22:16 +0000</pubDate>
		<dc:creator><![CDATA[admin]]></dc:creator>
				<category><![CDATA[2014]]></category>
		<category><![CDATA[Case Studies]]></category>

		<guid isPermaLink="false">http://productivity.imtma.in/?p=288</guid>
		<description><![CDATA[Energy Consumption Reduction in KB-Machine Shop]]></description>
				<content:encoded><![CDATA[<p><span style="color: #3572ad;"><strong>Title of case study:</strong></span><br />
Energy Consumption Reduction in KB-Machine Shop</p>
<p><span style="color: #3572ad;"><strong>Project implementation start and end date:</strong></span><br />
April 2013 to March 2014</p>
<p><span style="color: #3572ad;"><strong>Is it in continued operation now?:</strong></span> Yes</p>
<p><span style="color: #3572ad;"><strong>Problem identification: Why was this problem selected? What methodology was adopted to identify the problem?</strong></span><br />
Our management gave us a target of 5% reduction in electricity cost.<br />
Electricity is the major contributor of total cost in machine shop. It amounts to almost 40% of total cost.</p>
<p><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti1.jpg"><img class="alignnone size-medium wp-image-292" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti1-300x180.jpg" alt="maruti1" width="300" height="180" /></a><br />
The Energy cost has been increasing steadily over last few years due to increasing rates of power and fuel oil. The unit energy cost has raised by 31% in the last financial year.</p>
<p><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti2.jpg"><img class="alignnone size-full wp-image-293" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti2.jpg" alt="maruti2" width="218" height="96" /></a><br />
Hence the project on Energy consumption reduction was taken up.</p>
<p>Data collection: What data was collected? What methodology was adopted to collect the data?<br />
Histograms and Bar graphs were used to do analyse the monthly and daily Electricity consumption of shop and individual lines.</p>
<p><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti3.jpg"><img class="alignnone size-full wp-image-294" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti3.jpg" alt="maruti3" width="288" height="135" /></a><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti4.jpg"><img class="alignnone size-medium wp-image-295" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti4-300x113.jpg" alt="maruti4" width="300" height="113" /></a></p>
<p><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/MarutiGraph.png"><img class="alignnone size-medium wp-image-308" src="http://productivity.imtma.in/wp-content/uploads/2015/01/MarutiGraph-300x110.png" alt="MarutiGraph" width="300" height="110" /></a></p>
<p><span style="color: #3572ad;"><strong>Analysis and development of solution: What analysis was done? What alternate solutions were identified? Why was this particular solution chosen?</strong></span><br />
Based on the data collected, Energy consumption monitoring was divided into two parts:</p>
<ul>
<li>Off-time Energy Consumption reduction: Holiday and Break-time Consumption monitoring.</li>
<li>Line Running time Energy consumption: Day-wise Consumption monitoring</li>
</ul>
<p><span style="color: #3572ad;"><strong>Line Running time Energy consumption: Combined tool Development</strong></span></p>
<ul>
<li>Redistribution of operation.</li>
<li>Machine wise process study for understanding the power supply requirement</li>
<li>Machine auxiliary capacity checking for rationalization of pumps</li>
<li>VA/VE drive for idea generation for component weight reduction</li>
<li>One equipment – one second drive for cycle-time reductio</li>
</ul>
<p><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti7.jpg"><img class="alignnone size-medium wp-image-298" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti7-300x105.jpg" alt="maruti7" width="300" height="105" /></a></p>
<p><span style="color: #3572ad;"><strong>Off-time Energy <span style="color: #3572ad;">Consumption</span> reduction:</strong></span></p>
<ul>
<li>Layout checking and mapping with objective of auxiliary running as per production plan.
<ul>
<li>Air-washer</li>
<li>Exhaust fans</li>
<li>Air-supply</li>
<li>Centralized coolant system</li>
<li>Electrical Supply to individual lines</li>
</ul>
</li>
<li>Study of machines which cannot be switched off during holidays.</li>
</ul>
<p style="padding-left: 30px;">TABLE</p>
<p><span style="color: #3572ad;"><strong>Implementation: How was the chosen solution tested/validated and implemented?</strong></span></p>
<p><strong>Line Running Consumption Reduction:</strong></p>
<ul>
<li><strong>Combination tool development</strong>
<ul>
<li>Tool development for Crank bore roughing and Seat area machining simultaneously on one machine. (machine-100 + machine-90) sparing of one machine.</li>
<li>Increase in number of cutting edges of Tappet machining tool for reduced cycle time from 113 sec to 103 sec in machine-150 of cylinder head line.</li>
</ul>
</li>
</ul>
<p style="padding-left: 90px;"><img class="alignnone size-medium wp-image-299" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti8-300x163.jpg" alt="maruti8" width="300" height="163" /></p>
<p style="padding-left: 90px;">Operation optimization/Redistribution of operations.<br />
The head mounting hole spot facing operation of machine-40 were distributed to machine-70A and machine-70B in cylinder head line. This resulted in sparing of machine-40.</p>
<p style="padding-left: 90px;"><img class="alignnone size-medium wp-image-300" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti9-300x152.jpg" alt="maruti9" width="300" height="152" /></p>
<ul>
<li class="p2"><b>Optimization of Auxiliaries:</b>
<ul>
<li class="p2">Actual load and efficiency calculation</li>
<li class="p2">Checking of spare capacity, using formulae and NPSH graphs resulting in optimization of pump</li>
</ul>
</li>
</ul>
<p style="padding-left: 60px;"><img class="alignnone size-full wp-image-301" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti10.jpg" alt="maruti10" width="278" height="154" /> <img class="alignnone size-medium wp-image-302" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti11-300x142.jpg" alt="maruti11" width="300" height="142" /><br />
Sparing Chiller Units by clubbing units of Stand-alone Coolant Systems and connecting to Centralized Coolant system.</p>
<p style="padding-left: 60px;"><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti12.jpg"><img class="alignnone size-full wp-image-303" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti12.jpg" alt="maruti12" width="201" height="171" /></a></p>
<ul>
<li>
<ul>
<li>Interlocking of Hydraulic Power Packs and Mist-collectors with machine idling.</li>
<li>Optimization of Panel A/C temperature based on capacity:<br />
Energy saving for one degree change in set temperature was studied. Makers of the machines were contacted to know the respective optimum temperature setting.</li>
</ul>
</li>
<li><strong>VA/VE Ideas:</strong>
<ul>
<li>EGR hole extra boss was eliminated from component casting,</li>
<li>Raw material reduction in Holes of component raw material.</li>
<li><span style="line-height: 1.5;">These activities helped in reducing machining time, thus the cycle time.</span></li>
</ul>
</li>
<li><strong>Off-time Energy Consumption reduction:</strong>
<ul>
<li>Utility mapping and running as per requirement</li>
<li>Air-washer supply path was changed selective operation of during situations when only one of the two lines run.</li>
</ul>
</li>
</ul>
<p style="padding-left: 60px;"><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti13.jpg"><img class="alignnone size-medium wp-image-304" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti13-300x88.jpg" alt="maruti13" width="300" height="88" /></a></p>
<ul>
<li>Machining Lines were provided with individual Compressed air controllers so that during selective operation of lines, compressed air is not consumed by inactive lines.</li>
<li>Implementation of Switch-off plan for machines during off-time:</li>
</ul>
<p><span style="line-height: 1.5;">TABLE</span></p>
<p style="padding-left: 30px;"><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti14.jpg"><img class="alignnone size-medium wp-image-305" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti14-300x127.jpg" alt="maruti14" width="300" height="127" /></a></p>
<ul>
<li><span style="line-height: 1.5;">Timer control was done on utilities (Airwashers, Exhaust, Compressed Air) as per production plan.</span></li>
</ul>
<p style="padding-left: 30px;"><a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti16.jpg"><img class="alignnone size-full wp-image-307" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti16.jpg" alt="maruti16" width="175" height="98" /></a> <a href="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti15.jpg"><img class="alignnone size-full wp-image-306" src="http://productivity.imtma.in/wp-content/uploads/2015/01/maruti15.jpg" alt="maruti15" width="247" height="68" /></a></p>
<ul>
<li>The Quality Team of the shop and support functions of the lines were educated about these activities through display of Kaizen Sheets. All the changes which were directly affecting machining were updated in the Quality standard sheets. The Quality aspects were reviewed by:
<ul>
<li>Daily monitoring of trends and its review by top management</li>
<li>Display of changes on Change Point Control Board of the lines., Quality parameters were validated based on daily checking of components.</li>
<li><span style="line-height: 1.5;">Process change approvals were taken from respective engineering departments.</span></li>
</ul>
</li>
</ul>
<p><span style="color: #3572ad;"><strong>Has the solution been institutionalized? If yes, describe how briefly</strong></span><br />
The systems mentioned above have been institutionalized after implementation. The Process sheets related to the modifications were also Updated. These changes have been updated in the operational standards which were approved by the authorities.</p>
<p><span style="color: #3572ad;"><strong>Benefits to organization: What benefits accrued to the organization as a result of the implementation of the project?</strong></span></p>
<ol>
<li>Operational benefits: Describe the physical benefits from the project here:
<ul>
<li>The Productivity has increased by reduction of cycle time in the machines where the new tools were introduced.</li>
<li>The activities undertaken have resulted in Energy consumption reduction of 9% of total Energy over the period of one year.</li>
<li> The project aided the standardization of working parameters in auxiliary units of machines.</li>
</ul>
</li>
<li>Financial benefits: Describe the financial benefits directly attributable to this project here:<br />
Energy saving : Rs. 2.0 Crore</li>
</ol>
<p><span style="color: #3572ad;"><strong>Scope for horizontal deployment: Can the solution implemented in this project be deployed horizontally in other areas in the organization? Is there a scope to deploy this in other industries? Has any such deployment been made? If so describe.</strong></span></p>
<ul>
<li>The improvements done in the shops have been updated in the Central portal of Maruti where users from other shops/plants of Maruti can understand them.</li>
<li>Energy saving activities have been done in other shops/plants, sharing of ideas and successful improvements is an on-going activity.<br />
Entrants may give any other relevant information here that can prove helpful to make it a winning entry:</li>
<li>The Energy resources are depleting at a fast rate. We must devise innovative ways to address this issue. The activities mentioned above are a part of our continuous effort towards this cause.</li>
</ul>
]]></content:encoded>
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		<title>Productivity improvement in “Inline Fuel Injection Pump” value stream to ensure product profitability</title>
		<link>https://productivity.imtma.in/bosch/</link>
		<comments>https://productivity.imtma.in/bosch/#comments</comments>
		<pubDate>Tue, 20 Jan 2015 12:27:36 +0000</pubDate>
		<dc:creator><![CDATA[admin]]></dc:creator>
				<category><![CDATA[2014]]></category>
		<category><![CDATA[Case Studies]]></category>

		<guid isPermaLink="false">http://productivity.imtma.in/?p=262</guid>
		<description><![CDATA[Productivity improvement in “Inline Fuel Injection Pump” value stream to ensure product profitability]]></description>
				<content:encoded><![CDATA[<h3><span style="color: #3572ad;"><strong>Company:</strong> </span>BOSCH Limited</h3>
<h3><span style="color: #3572ad;"><strong>Project initiation date:</strong></span> Jun 2012</h3>
<h3><span style="color: #3572ad;"><strong>Challenge</strong></span></h3>
<p>Inline pump is Key product for Bangalore Plant and it has reached maturity stage of its life cycle. To ensure competitiveness and market share there is tremendous cost pressure on this product. Hence productivity improvement was selected as key measure.</p>
<ul>
<li>Higher lead time and reduced output due to crisis-cross flow of Pumps in post assembly operations (Phasing, Calibration, pre packing and Q-Screen Operations)</li>
</ul>
<ul>
<li>Non value added activities in DV Holder Line</li>
</ul>
<ul>
<li>Process oriented layout resulting in production failure to pump assembly, high inventory of camshaft.</li>
</ul>
<ul>
<li>Lower FPY in assembly and sub assembly processes across value stream</li>
</ul>
<ul>
<li>Consistent but low OEE (Benchmarking-DS/Brumschist) of Critical/Bottleneck machine</li>
</ul>
<ul>
<li>Low type wise delivery fulfillment to customers</li>
</ul>
<ul>
<li>Supplier delivery performance not up to the mark</li>
</ul>
<p>To resolve above issues we have used various quality/management tools like: Pareto analysis, Ishikawa Diagram, Bubble Diagram</p>
<p>In line with our plant vision we have used Brainstorming, System CIP workshop and KPI tree methodology to identify and prioritize focus areas. It also helped us in aligning our actions with targets. KPI tree, Lean Line Design (LLD), E-Kanban and consumption based production. Brummschicht</p>
<h3><span style="color: #3572ad;"><strong>Data Collection</strong></span></h3>
<p>Data collection through Value Stream Mapping and Bubble Diagram for Assembly line integration and LLD in DV holder.</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-1Bosch-22014-e1428299036864.jpg" target="_blank"><img class="alignnone wp-image-791 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-1Bosch-22014-e1428299036864-300x189.jpg" alt="Figure 1Bosch 22014" width="300" height="189" /></a></p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-2Bosch-22014-e1428299801245.jpg" target="_blank"><img class="alignnone wp-image-792 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-2Bosch-22014-e1428299801245-300x234.jpg" alt="Figure 2Bosch 22014" width="300" height="234" /></a></p>
<p>Production data and losses were collected through hourly Monitoring sheet. Pareto chart was used identifying top losses. (in Camshaft Grinding and T- bolt Honing M/c)</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-3Bosch-22014-e1428299843847.jpg" target="_blank"><img class="alignnone wp-image-793 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-3Bosch-22014-e1428299843847-300x240.jpg" alt="Figure 3Bosch 22014" width="300" height="240" /></a></p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-4Bosch-22014-e1428300020303.jpg" target="_blank"><img class="alignnone wp-image-794 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-4Bosch-22014-e1428300020303-300x211.jpg" alt="Figure 4Bosch 22014" width="300" height="211" /></a></p>
<p>(Autocal data collection for FPY improvement in Calibration)</p>
<h3><span style="color: #3572ad;"><strong>Analysis and Solution Development</strong></span></h3>
<p>MTM Analysis, Stack diagram &amp; Operator Balance chart were used to improve material flow and operator movements in assembly line integration and LLD and Cellular manufacturing.</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-5Bosch-22014-e1428300051999.jpg" target="_blank"><img class="alignnone wp-image-795 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-5Bosch-22014-e1428300051999-300x265.jpg" alt="Figure 5Bosch 22014" width="300" height="265" /></a></p>
<p>Application of Shainin method to analyze the major rejections in calibration and also use of “Error – Contribution Matrix” to zero in on top contributors</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-6Bosch-22014-e1428300078313.jpg" target="_blank"><img class="alignnone wp-image-796 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-6Bosch-22014-e1428300078313-300x167.jpg" alt="Figure 6Bosch 22014" width="300" height="167" /></a></p>
<p>PDCA and Problem solving sheet (PSS) were used to analyze and develop solutions as a part of SFMC approach in critical and bottleneck machines.</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-7Bosch-22014-e1428300106364.jpg" target="_blank"><img class="alignnone wp-image-797 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-7Bosch-22014-e1428300106364-300x208.jpg" alt="Figure 7Bosch 22014" width="300" height="208" /></a></p>
<h3><span style="color: #3572ad;"><strong>Solution</strong></span></h3>
<p>KPI Tree approach for analyze and develop solution for improve type wise fulfillment.</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-8Bosch-22014-e1428300131946.jpg" target="_blank"><img class="alignnone wp-image-798 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-8Bosch-22014-e1428300131946-300x212.jpg" alt="Figure 8Bosch 22014" width="300" height="212" /></a></p>
<h3><span style="color: #3572ad;"><strong>Implementation</strong></span></h3>
<p>Solutions related to Line integration, LLD and Cellular Manufacturing were validated using “Mock Line Layout” Methodology. (Before-After)</p>
<p>Eg: DV holder - Optimization from 6 stations to 3 stations, FIFO between the stations established</p>
<p>Assembly line - External U line converted to internal U</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-9Bosch-22014-e1428300157829.jpg" target="_blank"><img class="alignnone wp-image-799 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-9Bosch-22014-e1428300157829-300x240.jpg" alt="Figure 9Bosch 22014" width="300" height="240" /></a></p>
<p>Following 6 Kaizens were implemented during FPY improvement across value stream. Solutions were validated using Shainin tool paired comparison.</p>
<p>Eg: Modifications in design of Base cup mandrel eliminate contact between O- ring and adhesive &amp; reduce replacement cost.</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-10Bosch-22014-e1428300192174.jpg" target="_blank"><img class="alignnone wp-image-800 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-10Bosch-22014-e1428300192174-300x198.jpg" alt="Figure 10Bosch 22014" width="300" height="198" /></a></p>
<p>OEE improvement done through SMC approach and validated using layered process Confirmation (LPC). Eg: Technical losses reduction by optimization of spindle parameters in honing m/c and honing stone specifications.</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-11Bosch-22014-e1428300218473.jpg" target="_blank"><img class="alignnone wp-image-801 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-11Bosch-22014-e1428300218473-300x235.jpg" alt="Figure 11Bosch 22014" width="300" height="235" /></a></p>
<h3><span style="color: #3572ad;"><strong>Sustain</strong></span></h3>
<p>Yes,</p>
<p>Layout, Work instruction chart and Standardized Worksheet for</p>
<p>Operators,updated based on improvements done in camshaft and calibration</p>
<p>area.Updation of documents like drawing, Control Plan, FMEA etc. done in</p>
<p>Pump Assembly and DV Holder assembly Line</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-12Bosch-22014-e1428300247437.jpg" target="_blank"><img class="alignnone wp-image-802 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-12Bosch-22014-e1428300247437-300x210.jpg" alt="Figure 12Bosch 22014" width="300" height="210" /></a></p>
<h3><span style="color: #3572ad;"><strong>Benefits</strong></span></h3>
<p>Overall Productivity increase from 0.3 to 0.37 pcs/man-hour by line Integration and lean line design</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-13Bosch-22014.jpg" target="_blank"><img class="alignnone wp-image-803 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-13Bosch-22014-e1428300352278-277x300.jpg" alt="Figure 13Bosch 22014" width="277" height="300" /></a></p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-14Bosch-22014-e1428300323854.jpg" target="_blank"><img class="alignnone wp-image-804 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-14Bosch-22014-e1428300323854-300x222.jpg" alt="Figure 14Bosch 22014" width="300" height="222" /></a></p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-15Bosch-22014-e1428300384372.jpg" target="_blank"><img class="alignnone wp-image-805 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-15Bosch-22014-e1428300384372-300x271.jpg" alt="Figure 15Bosch 22014" width="300" height="271" /></a></p>
<h3><span style="color: #3572ad;"><strong>Financial benefits</strong></span></h3>
<p>Direct Cost Saving = 46.1 mINR/annum</p>
<p>Avoidance of Investments= 27.5 mINR D</p>
<p>V Holder: 2.5 mINR</p>
<p>Honing machine: 25.0 mINR</p>
<h3><strong><span style="color: #3572ad;">Production</span></strong></h3>
<ol>
<li>a) 2012: 7,40,177 Pumps</li>
<li>b) 2013: 8,06,381 Pumps</li>
<li>c) Additional business: Export market 16,000 pumps/annum d) Rationalization of Manpower</li>
</ol>
<h3><span style="color: #3572ad;"><strong>Horizontal deployment</strong></span></h3>
<p>Considering Lessons learnt from successful Implementation of Line Integration and LLD; Horizontal deployment extended in Flyweight and Gov. cover subassembly Value Streams. OEE and FPY improvement projects are also initiated in rest of the processes/VS</p>
<p>Success stories have been shared with other VS and cross-functional teams through weekly Continuous Improvement Process (CIP) and Shop Floor CIP (SFC) Presentations.</p>
<p>Achievements have been shared and awards received at many industry platforms like NCQC, CCQC, QCFI and NIQR .</p>
<h3><span style="color: #3572ad;"><strong>Other inputs</strong></span></h3>
<p>Many lean initiatives have also been implemented in indirect areas through VSDiA (Value Stream Design in Indirect Areas).</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-16Bosch-22014-e1428300413540.jpg" target="_blank"><img class="alignnone wp-image-806 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-16Bosch-22014-e1428300413540-300x242.jpg" alt="Figure 16Bosch 22014" width="300" height="242" /></a></p>
<p>Below mentioned change initiatives has also helped the value stream to progress in the direction of achieving our plant Vision</p>
<p><a href="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-17Bosch-22014-e1428300443639.jpg" target="_blank"><img class="alignnone wp-image-807 size-medium" src="https://productivity.imtma.in/wp-content/uploads/2015/04/Figure-17Bosch-22014-e1428300443639-296x300.jpg" alt="Figure 17Bosch 22014" width="296" height="300" /></a></p>
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		<title>Productivity improvement in BDN Nozzle manufacturing line</title>
		<link>https://productivity.imtma.in/msdelphi-tvsdiesel/</link>
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		<pubDate>Sat, 17 Jan 2015 08:13:05 +0000</pubDate>
		<dc:creator><![CDATA[admin]]></dc:creator>
				<category><![CDATA[2014]]></category>
		<category><![CDATA[Case Studies]]></category>
		<category><![CDATA[Champion Award Winner 2014]]></category>

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		<description><![CDATA[Productivity improvement in BDN Nozzle manufacturing line to meet the sudden increase in customer demand (TML Passenger car and LTV market).]]></description>
				<content:encoded><![CDATA[<div class="imtma-abstract"><img class="alignnone wp-image-811" src="https://productivity.imtma.in/wp-content/uploads/2015/04/04_01_2014AwardImage.jpg" alt="04_01_2014AwardImage" width="750" height="176" /></div>
<div class="imtma-abstract"></div>
<h3 class="imtma-abstract"><strong><span style="color: #3572ad;">Title</span>:</strong> Productivity improvement in BDN Nozzle manufacturing line to meet the sudden increase in customer demand (TML Passenger car and LTV market).</h3>
<div class="imtma-abstract">
<h3><span style="color: #3572ad;"><strong>Company:</strong> </span>Delphi – TVS Diesel systems Ltd</h3>
<h3><span style="color: #3572ad;"><strong>Project initiation date:</strong> </span>10/10/2012</h3>
<h3><span style="color: #3572ad;"><strong>Challenge </strong></span></h3>
<p>Productivity improvements are the need of hour for the BDN nozzle manufacturing line to meet the sudden increase in customer demand from 2800 nos / day to 4000 nos / day . Current capacity of the line is 3000 nos / day. To meet the increased customer demand it requires investment around 4 crores and also high lead time     ( 12 months ) for procurement of new machines. Hence planned to increase the capacity without investment through productivity improvements to meet the increased customer demand.</p>
<p>Also used the takt time vs capacity analysis to identify the above problem.</p>
<h3><span style="color: #3572ad;"><strong>Data Collection</strong></span></h3>
<p>Following data was collected to understand the current status.</p>
<ul>
<li>Customer demand month wise</li>
<li>Process flow</li>
<li>Current capacity of each process</li>
<li>Up time of critical machines</li>
<li>Rejection levels in each process</li>
<li>Current manufacturing system</li>
<li>Current state of layout</li>
<li>Used the lean manufacturing methodology to collect the data like VALUE Stream Mapping, Cycle time study, Material flow – Sting diagram, Trend graph, Histogram/paretto</li>
</ul>
<h3><span style="color: #3572ad;"><strong>Analysis and Solution Development</strong></span></h3>
<p>BDN nozzle manufacturing process consists of 2 stages. Each stage has several sub processes. We have drawn the VSM for each stage to identify the bottle necks in the flow.</p>
<p><strong>Figure 1</strong></p>
<p><strong>Figure 2</strong></p>
<p>The following bottlenecks were identified in the BDN nozzle-manufacturing stream Cycle time is higher than takt time in ECM process</p>
<p>More unwash rejections observed in seat forming process at soft stage resulting FTPR low in downstream processes</p>
<p>Concentricity and linear dimensional issues in OD grinding operation resulting FTPR low in downstream processes.</p>
<p>Up time low in SEIKO ID grinding operation</p>
<p>Batch type production and process type layout is followed in hard stage machining leads to</p>
<p>More material movement</p>
<p>More operator movement for inspection</p>
<p>More handling – re handling</p>
<p>More WIP between process</p>
<p>Difficulties in day-to-day planning</p>
<p>More supervision required</p>
<p>Due to the above constraints it was unable to meet the increased customer demand.</p>
<h3><span style="color: #3572ad;"><strong>Solution</strong></span></h3>
<p>To eliminate the above listed constraints developed the various ideas through CFT approach as below.</p>
<p><strong>Figure 3</strong></p>
<h3><span style="color: #3572ad;"><strong>Implementation</strong></span></h3>
<p><strong>Figure 4</strong></p>
<p><strong>Figure 5</strong></p>
<p><strong>Figure 6</strong></p>
<p><strong>Figure 7</strong></p>
<p><strong>Figure 8</strong></p>
<p>Cellular layout formed by physical arrangement of machines according to the process flow.</p>
<p>Single piece flow between each process, material handling system modified, dedicated inspection facility provided, dedicated team formed from various functions and training given to the team about cellular concepts</p>
<h3><span style="color: #3572ad;"><strong>Sustain</strong></span></h3>
<p>Have standardized the actions taken to sustain the results through Control plan, Operation layout, Drawing Machineries layout document and Engineering change request / process change request</p>
<h3><span style="color: #3572ad;"><strong>Benefits</strong></span></h3>
<p><strong>Figure 9</strong></p>
<p>Elimination of working on Sundays resulted in power units saving – 60000 units/month and manpower saving - 20 people/day</p>
<h3><span style="color: #3572ad;"><strong>Financial benefits</strong></span></h3>
<p><strong>Figure 10</strong></p>
<p>Total cost saving/year - 1.51 crores and investment for new machine – 4 crores avoided</p>
<h3><span style="color: #3572ad;"><strong>Horizontal deployment</strong></span></h3>
<p>Learning of cellular layout concept with single piece flow can be adopted for pump manufacturing stream.</p>
<p>Learning of hard turning operation implemented in pump delivery valve OD turning process.</p>
<h3><span style="color: #3572ad;"><strong>Other inputs</strong></span></h3>
<p>The team implemented cellular layout with the centralized coolant tank and chillers outside the air condition room which helped in creating dust, mist and fumes free environment (EOHS improvement). Operators are voluntarily coming to work in the newly formed layout and also information flow between customer and supplier process is improved. There is substantial increase in morale of workmen in entire nozzle manufacturing stream.</p>
<p><strong>Figure 11</strong></p>
</div>
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